ASN Wikibase Occurrence # 167896
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Date: | Sunday 13 July 2014 |
Time: | 13:00 |
Type: | Piper PA-28-181 Arrow II |
Owner/operator: | Wisconsin Fox River Flyers Inc |
Registration: | N9681K |
MSN: | 28-7690274 |
Year of manufacture: | 1976 |
Total airframe hrs: | 7291 hours |
Engine model: | Lycoming O&VO-360 SER |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | near Waukesha Airport, Waukesha, WI -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Watertown, WI (RYV) |
Destination airport: | Waukesha Airport, WI (UES/KUES) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that he had entered the airport traffic pattern for landing. When the airplane was abeam the approach end of the runway, he reduced power, applied carburetor heat, and confirmed that the auxiliary fuel pump was on. When the airplane was on the base leg of the traffic pattern, the pilot attempted to increase engine power, but the engine did not respond; he stated that advancing the throttle to full did not result in an increase in power. He attempted moving the engine and carburetor heat controls to no avail. While attempting the remedial action, he turned toward the runway and declared an emergency. The airplane impacted trees short of the runway. A postaccident examination of the airplane confirmed that fuel was present. The engine was rotated and compression was verified on all cylinders, and the magnetos showed spark that was confirmed at all of the spark plug leads. No mechanical reason for the loss of engine power was discovered. At the time of the accident, the temperature and dew point were 24 degrees C and 17 degrees C, respectively. According to a carburetor icing probability chart, the temperature and dew point were in a range of susceptibility for moderate icing at cruise power settings and serious icing at descent power settings. Because the pilot reported using carburetor heat during the landing approach, the reason for the loss of engine power could not be determined.
Probable Cause: The loss of engine power for reasons that could not be determined because no anomalies were identified during postaccident examination.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN14LA443 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
https://flightaware.com/resources/registration/N9681K Location
Revision history:
Date/time | Contributor | Updates |
13-Jul-2014 23:49 |
Geno |
Added |
15-Jul-2014 10:40 |
winstell |
Updated [Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
30-Nov-2017 18:53 |
ASN Update Bot |
Updated [Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
08-Nov-2022 05:57 |
Ron Averes |
Updated [Location, Destination airport, Source] |
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