ASN Wikibase Occurrence # 168259
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Date: | Tuesday 5 August 2014 |
Time: | 11:15 |
Type: | Pitts S-2B |
Owner/operator: | Lance Murray Aviation Llc |
Registration: | N88EW |
MSN: | 5073 |
Year of manufacture: | 1985 |
Total airframe hrs: | 1330 hours |
Engine model: | Lycoming AEIO-540-D4A5 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near Oceanside Municipal Airport (KOKB), Oceanside, California -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Carlsbad, CA (CRQ) |
Destination airport: | Carlsbad, CA (CRQ) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that, following spin practice in a local practice area, he leveled the airplane and noticed that the bubble within the fuel sight gauge was not visible. As the pilot began to return to the departure airport, the engine began to run rough. The pilot immediately diverted to a nearby airport, and, shortly after diverting, the engine lost power. The pilot performed a left circling approach to the runway; however, he realized he was too high as he turned onto the base leg of the traffic pattern. The pilot then performed a left sideslip to increase the rate of descent. He did not think that he was in a safe position to land and performed a right 270-degree turn. The pilot stated that, during the turn, he realized the airplane would not be able to reach the runway, and he initiated a forced landing to an open field. Subsequently, the airplane landed hard and nosed over. The pilot reported that before the flight he thought that he had three-quarters of a tank of fuel onboard the airplane, which he thought was sufficient for a 30-minute flight plus visual flight rules reserve fuel requirements.
Postaccident examination of the airplane revealed that when the main fuel tank fuel cap was removed, about 1 to 2 cups of liquid drained from the fuel tank. The engine was test run while installed on the airframe without incident. In addition, the fuel indicating system was found to function normally and no leaks were observed within the fuel system. Further examination of the airplane revealed no preexisting mechanical anomalies that would have precluded normal operation.
Probable Cause: The total loss of engine power due to fuel exhaustion. Contributing to the accident was the pilot’s inadequate fuel planning.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR14LA329 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=88EW
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
05-Aug-2014 23:04 |
Geno |
Added |
08-Aug-2014 00:52 |
Geno |
Updated [Source] |
28-Aug-2014 07:03 |
lanceav8r |
Updated [Narrative] |
28-Aug-2014 07:04 |
harro |
Updated [Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
30-Nov-2017 18:58 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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