ASN Wikibase Occurrence # 170099
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Date: | Tuesday 23 September 2014 |
Time: | 20:10 |
Type: | Piper PA-31T Cheyenne II |
Owner/operator: | American Medflight Inc |
Registration: | N774MF |
MSN: | 31T-7920035 |
Year of manufacture: | 1979 |
Engine model: | P&W Canada PT6A-60A |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Oakland International Airport (KOAK), Oakland, CA -
United States of America
|
Phase: | Landing |
Nature: | Ambulance |
Departure airport: | Reno, NV (KRNO) |
Destination airport: | Oakland, CA (OAK) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that while on an instrument landing system (ILS) approach for the medical life-flight, he was struggling to keep the airplane on the localizer and glide path. As the airplane descended through 800 to 900 feet above the ground, he broke out of the cloud layer but had difficulty locating the runway in the dark night conditions. During the landing flare he reduced the throttle and as the airplane touched down on the runway surface, he realized the landing gear were retracted; he did not hear any horns. The pilot recalled that when he selected the landing gear, he may have put the handle in neutral rather than keeping his hand on the lever and waiting for the three green lights to illuminate confirming the extended position. He did not follow his normal checklists because of the demands of the ILS approach. He also cited a few stressors in his life that may have contributed to a distraction including a change of airplanes and few ILS approaches performed in the recent six months. The pilot further added that there were no pre impact mechanical malfunctions or failures that would have precluded normal operation. The airplane incurred substantial damage to the lower fuselage and engine mounts.
Probable Cause: The pilot's failure to extend the landing gear which resulted in a gear-up landing. Contributing to the accident was the pilot's failure to use the checklist and reported stress.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR14CA391 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N774MF Location
Revision history:
Date/time | Contributor | Updates |
24-Sep-2014 16:03 |
Geno |
Added |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
30-Nov-2017 19:10 |
ASN Update Bot |
Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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