ASN Wikibase Occurrence # 173749
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Date: | Wednesday 11 February 2015 |
Time: | 14:33 |
Type: | Wheeler Express |
Owner/operator: | Private |
Registration: | N564ER |
MSN: | XP0123 |
Year of manufacture: | 2013 |
Total airframe hrs: | 14 hours |
Engine model: | Lycoming IO-540-S1A5 |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | SE of Greeley-Weld County Airport (KGXY), Greeley, CO -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Greeley, CO (GXY) |
Destination airport: | Denver, CO (FTG) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot/owner of the experimental amateur-built airplane and an airline transport pilot-rated passenger arrived at an airport, and a mechanic heard the engine backfiring and "missing." The pilots subsequently stated to the mechanic that they had been experiencing problems with the engine. The mechanic offered that his boss could look at the engine, but the pilots did not want to wait. The mechanic accompanied the pilots to the airplane, and helped them start it with auxiliary power. They then realized the starter solenoid was not engaging the starter. About 10 minutes later, the pilot requested a jumper wire to bypass the the starter solenoid in order to start the engine. The engine started, and, as the airplane taxied for takeoff, the mechanic noted that the engine was still running rough.
A witness, who was located about 3/4 mile from the accident location, reported hearing the airplane's engine "sputtering." When the airplane flew over about 200-300 ft above ground level, the engine was running rough and occasionally "missing." He then heard the engine stop running and saw the airplane subsequently descend about 30° nose-low into an open field at high speed.
There was an immediate postimpact fire. An examination of the airplane, engine, and other airplane systems revealed no anomalies.
The pilot had not completed a flight review in over 7 years; had not logged any flight time in the 2 years before the accident; and his recency of flight experience, including the last time he may have practiced emergency procedures, could be determined. Although the reason for the loss of engine power could not be determined during postaccident examination, the high-speed, nose-low impact is consistent with a loss of airplane control.
Probable Cause: The pilot's failure to maintain airplane control during an off-airport forced landing following a total loss of engine power for reasons that could not be determined during postaccident examination of the engine. Contributing to the accident was the pilots' decision to conduct the flight with known mechanical deficiencies.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN15FA141 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N564ER Location
Revision history:
Date/time | Contributor | Updates |
12-Feb-2015 00:50 |
Geno |
Added |
12-Feb-2015 17:02 |
Geno |
Updated [Registration, Cn, Operator, Source, Narrative] |
24-Feb-2015 16:40 |
Geno |
Updated [Time, Phase, Nature, Departure airport, Destination airport, Source, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
17-May-2017 17:27 |
PiperOnslaught |
Updated [Source, Narrative] |
19-Aug-2017 14:59 |
ASN Update Bot |
Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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