Loss of control Accident Rans S-12 Airaile N154BH,
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ASN Wikibase Occurrence # 174344
 
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Date:Saturday 7 March 2015
Time:12:30
Type:Silhouette image of generic RS12 model; specific model in this crash may look slightly different    
Rans S-12 Airaile
Owner/operator:Private
Registration: N154BH
MSN: 0195553
Year of manufacture:1995
Total airframe hrs:1406 hours
Engine model:Bombardier Rotax
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Near Cherokee County Airport (KJSO), Jacksonville, TX -   United States of America
Phase: Approach
Nature:Private
Departure airport:Rusk, TX (JSO)
Destination airport:Rusk, TX (JSO)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The passenger had purchased the experimental amateur-built airplane about 2 weeks before the accident flight and was conducting a familiarization flight with a private pilot. The pilot had about 11,000 hours of total flight time, with about 2 hours in the accident make and model. Witnesses reported that the airplane was conducting touch and go takeoffs and landings but that the engine did not sound normal. They subsequently saw the airplane maneuver toward a field before it stalled, collided with trees, and impacted the ground. There was evidence of fuel at the accident site, and inspection of the airframe and engine did not reveal any abnormalities. According to the carburetor icing probability chart, the airplane was operating in an environment conducive to light carburetor icing at cruise or descent power; it is unlikely that the loss of engine power was the result of carburetor ice accumulation. The reason for the loss of engine power could not be determined based on available information.



Probable Cause: A partial loss of engine power for reasons that could not be determined based on the available information. Contributing to the accident was the pilot's failure to maintain control while maneuvering for a forced landing, which resulted in the airplane exceeding its critical angle of attack and experiencing an aerodynamic stall.


Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN15LA169
Status: Investigation completed
Duration: 3 years
Download report: Final report

Sources:

NTSB
FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=154BH

Location

Revision history:

Date/timeContributorUpdates
08-Mar-2015 05:18 Geno Added
08-Mar-2015 07:46 Geno Updated [Aircraft type, Operator, Source, Narrative]
09-Mar-2015 21:58 Geno Updated [Aircraft type, Registration, Cn, Source, Narrative]
16-Jan-2016 19:29 Anon. Updated [Damage]
21-Dec-2016 19:28 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
24-Mar-2018 18:40 ASN Update Bot Updated [Nature, Departure airport, Destination airport, Source, Narrative]

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