Accident Cessna 172M Skyhawk N12842,
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ASN Wikibase Occurrence # 175401
 
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Date:Tuesday 14 April 2015
Time:13:45
Type:Silhouette image of generic C172 model; specific model in this crash may look slightly different    
Cessna 172M Skyhawk
Owner/operator:Private
Registration: N12842
MSN: 172-62306
Year of manufacture:1973
Total airframe hrs:8251 hours
Engine model:Lycoming O-320-D2J
Fatalities:Fatalities: 0 / Occupants: 3
Aircraft damage: Substantial
Category:Accident
Location:Hilo Airport, Hawaii, HI -   United States of America
Phase: Take off
Nature:Training
Departure airport:Hilo International Airport, HI (ITO/PHTO)
Destination airport:Hilo International Airport, HI (ITO/PHTO)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The flight instructor and pilot receiving instruction reported that, during the preflight inspection before the local instructional flight, they drained water from the fuel tanks. After departure, they flew for about 1 hour and then returned to the airport to practice touch-and-go landings. During the approach for landing, the pilot receiving instruction accomplished a no-flap “slip to landing.” After touchdown, he applied power for the takeoff, and the airplane then reached between about 75 and 100 ft above ground level, at which point the engine began to run irregularly, and subsequently, it lost power. The flight instructor took control of the airplane and executed a left turn away from buildings located at the end of the runway. Subsequently, the airplane impacted a grassy area northeast of the departure end of the runway.
During the postaccident examination of the airplane, water was found in the fuel sump strainer and the carburetor, which likely led to the loss of engine power. It is likely the flight instructor and pilot receiving instruction failed to ensure that all the water was drained from the tank during the preflight inspection.


Probable Cause: Water contamination in the fuel system due to the flight instructor’s and pilot receiving instruction’s failure to drain all the water from the system during the preflight inspection, which resulted in a loss of engine power.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR15LA146
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB
FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=12842

Location

Revision history:

Date/timeContributorUpdates
15-Apr-2015 01:29 Geno Added
15-Apr-2015 03:49 Geno Updated [Aircraft type, Registration, Cn, Operator, Nature, Source, Narrative]
15-Apr-2015 06:06 Anon. Updated [Aircraft type, Registration, Cn, Operator]
15-Apr-2015 13:39 Geno Updated [Operator, Nature, Source, Narrative]
19-Apr-2016 19:54 Anon. Updated [Location, Narrative]
21-Dec-2016 19:30 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
12-Dec-2017 20:01 ASN Update Bot Updated [Time, Operator, Nature, Departure airport, Destination airport, Source, Narrative]
09-Jun-2023 14:50 Ron Averes Updated [[Time, Operator, Nature, Departure airport, Destination airport, Source, Narrative]]

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