ASN Wikibase Occurrence # 177196
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Date: | Monday 3 May 2004 |
Time: | 20:30 |
Type: | Beechcraft 65 Queen Air LF-23F |
Owner/operator: | Quueenaire Incorporated |
Registration: | N870KS |
MSN: | LF-9 |
Total airframe hrs: | 1213 hours |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Winder, GA -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Lawrenceville-Gwinnett County Briscoe Field, GA (LZU/KLZU) |
Destination airport: | Winder Airport, GA (WDR/KWDR) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that the airplane lost power in the right engine first, and the left engine lost power approximately thirty seconds later. Efforts by the pilot to restart the engines were unsuccessful. The airplane collided with the ground one mile southeast of Winder Barrow County Airport. Prior to the flight, the pilot reported that the airplane had intermediate magneto drops in power. Examination of the fuel tanks revealed that both inboard main fuel tanks were empty. Both auxiliary fuel tanks were approximately half full. Trace amounts of fuel were recovered from the left fuel line and no fuel was recovered from the right fuel line. During the examination of the airplane, no fuel leakage or fuel stains were observed on the airframe. Further examination of the airplane revealed the right fuel selector was in the main detent position, and the left fuel selector was observed 15 degrees away from the main detent position. Further examination of the engines revealed that both fuel sumps were damaged. External examination of both engines revealed full intake and exhaust valve action, internal component rotation was accomplished, and compression and suction in all cylinders were noted. Both fuel flow dividers were dry and free of debris when examined. The magnetos were checked for internal and engine timing; both engine magnetos were within prescribed limits. Also, both engine magnetos produced ignition sparks on all ignition leads when rotated.
Probable Cause: The pilot's mismanagement of the fuel supply resulted in fuel starvation and a loss of power in both engines.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL04CA106 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20040608X00745&key=1 Location
Revision history:
Date/time | Contributor | Updates |
22-Jun-2015 16:39 |
Noro |
Added |
21-Dec-2016 19:30 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
07-Dec-2017 18:43 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
17-Nov-2022 20:49 |
Ron Averes |
Updated [Aircraft type, Departure airport, Destination airport] |
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