Accident Aeronca 7AC N3708E,
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ASN Wikibase Occurrence # 177362
 
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Date:Saturday 8 May 2004
Time:18:22
Type:Silhouette image of generic CH7A model; specific model in this crash may look slightly different    
Aeronca 7AC
Owner/operator:Private
Registration: N3708E
MSN: 7AC-7009
Total airframe hrs:1985 hours
Engine model:Lycoming O-235
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Fort Stockton, TX -   United States of America
Phase: Landing
Nature:Private
Departure airport:Van Horn, TX (VHN)
Destination airport:Fort Stockton, TX (FST)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The 821-hour commercial pilot lost engine power while in cruise flight at 2,500 feet mean sea level approximately 25 miles west of his intended destination. While en route, he noticed the oil temperature gauge indicated 240 degrees (red line was 145 degrees). The pilot reduced engine rpm from 2,400 to 2,200, and increased the airplane's mixture setting. The oil temperature began to decrease. Shortly after, the engine suddenly began to lose power. The pilot increased the mixture setting to "full rich", and applied carburetor heat, but the engine continued to lose power. He was unable to maintain altitude and executed a forced landing to a service road on Interstate 10. Upon landing, the pilot was unable to keep the airplane straight due to the strong, gusting crosswinds and collided with a metal fence post and mesquite trees. Examination of the top and bottom spark plugs revealed the #2 and #4 plugs were oily, and the #1 and #3 plugs appeared white in color. The oil, which was changed approximately 8 hours before the accident, was dark in color. When asked how this accident could have been prevented, the pilot reported, "I probably leaned engine too much too long causing the oil temp[erature] to reach 240 degrees. Run aircraft more rich to provide better cooling to internal combustion chambers." Weather reported at an airport about 17 miles from the accident site were reported as wind from 130 degrees at 17 knots gusting to 24 knots.
Probable Cause: The pilot's improper leaning of the fuel/air mixture in-flight, which resulted in a loss of engine power. Factor were the wind gusts and the crosswind.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: FTW04LA124
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20040517X00607&key=1

History of this aircraft

Other occurrences involving this aircraft
1 June 1985 N3708E Joe David Sanders 0 Edna, TX sub

Location

Revision history:

Date/timeContributorUpdates
27-Jun-2015 20:19 Noro Added
21-Dec-2016 19:30 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
07-Dec-2017 18:02 ASN Update Bot Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative]

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