ASN Wikibase Occurrence # 17860
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Date: | Friday 16 May 2008 |
Time: | 11:53 |
Type: | Fairchild-Hiller FH-1100 |
Owner/operator: | Private |
Registration: | N5049F |
MSN: | 196 |
Year of manufacture: | 1970 |
Total airframe hrs: | 5012 hours |
Engine model: | Allison 250-C18B |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Chipman Preserve, Comstock Township, MI -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Kalamazoo, MI |
Destination airport: | Kalamazoo, MI |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot purchased the helicopter the day prior to the accident. He was returning to his home airstrip after having flown with a certified flight instructor when the accident occurred. A witness reported hearing a loss of engine noise followed by the impact. The helicopter contacted a 40-foot-tall tree and impacted the ground, coming to rest on its right side. The tree was located near a small clearing in a heavily wooded area. The wreckage was aligned with the end of the pilot's airstrip. Inspection of the helicopter, control systems, engine, and transmission, failed to reveal any anomalies that would have precluded normal operation of the helicopter. Fuel was not visible in the fuel tank. Approximately 2 quarts of fuel were drained from the tank following the accident. There was no evidence of a fuel spill/leak at the accident site. The helicopter has a usable fuel quantity of 66.9 gallons. It has an average cruise airspeed of 85 to 90 miles per hour and it consumes about 22 gallons per hour. The distance from where the helicopter was last fueled to the pilot's airstrip is approximately 82 miles. The pilot then flew approximately 22 miles from his airstrip to pick up his flight instructor. They then flew in the local area for about 1 hour. The certified flight instructor stated that the pilot had departed about 1100 to return to his airstrip. The accident occurred at 1153.
Probable Cause: A loss of engine power in flight due to fuel exhaustion resulting from the pilot's inadequate fuel management. Contributing to the accident was the unsuitable terrain for a forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI08FA132 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
17-May-2008 02:33 |
Fusko |
Added |
24-Jun-2017 17:03 |
Aerossurance |
Updated [Operator, Location, Destination airport] |
03-Dec-2017 12:47 |
ASN Update Bot |
Updated [Time, Cn, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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