ASN Wikibase Occurrence # 178635
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Date: | Saturday 8 August 2015 |
Time: | 10:15 |
Type: | Cessna 182Q Skylane |
Owner/operator: | Private |
Registration: | N7506S |
MSN: | 18265199 |
Year of manufacture: | 1976 |
Engine model: | Continental O-470 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Bath Alum Airport (9VA0), Warm Springs, VA -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Hot Springs, VA (HSP) |
Destination airport: | Wise, VA (LNP) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The non-pilot-rated passenger had recently purchased the airplane, which had not been flown in the previous 6 years and did not have a current annual inspection. He and his brother, a private pilot, were returning the airplane to their home airport. During the initial climb after takeoff, about 100 ft above ground level, the engine rpm “dropped”; the pilot landed on the remaining runway but was unable to stop the airplane before it departed the end of the runway and nosed over.
A postaccident examination revealed that the right magneto did not produce spark. It is likely that the magneto failed during the takeoff, resulting in the loss of engine power. The pilot reported that fuel sampled from the right wing tank before the accident flight had a green tint and postaccident photographs showed green staining on the right side fuselage consistent with a leak from the right wing. The source of the green tint was not determined; however, it likely did not affect engine operation since the fuel selector was set to the left fuel tank, which did not have any evidence of green-tinted fuel, and no green tint was observed in the fuel strainer.
Probable Cause: A partial loss of engine power during initial climb due to the failure of a magneto. Contributing to the accident was the pilot's decision to operate the airplane without a current annual inspection.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA15LA300 |
Status: | Investigation completed |
Duration: | 3 years 1 month |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=7506S Location
Images:
Photo: FAA
Revision history:
Date/time | Contributor | Updates |
14-Aug-2015 15:56 |
Geno |
Added |
21-Dec-2016 19:30 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
16-Sep-2018 19:11 |
ASN Update Bot |
Updated [Departure airport, Destination airport, Source, Narrative, Accident report, ] |
17-Sep-2018 19:11 |
harro |
Updated [Source, Narrative, Photo] |
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