Runway excursion Accident Cessna 421B Golden Eagle N813CA,
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ASN Wikibase Occurrence # 179775
 
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Date:Monday 21 September 2015
Time:10:40
Type:Silhouette image of generic C421 model; specific model in this crash may look slightly different    
Cessna 421B Golden Eagle
Owner/operator:Private
Registration: N813CA
MSN: 421B0894
Total airframe hrs:3844 hours
Engine model:Continental GTSIO-520 H1B
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Platteville Municiple Airport (KPVB), Platteville, WI -   United States of America
Phase: Take off
Nature:Executive
Departure airport:Platteville, WI (KPVB)
Destination airport:Dayton, OH (KDAY)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The commercial pilot reported that he completed the pretakeoff checklist, which included a run-up of each engine; no anomalies were noted. During the takeoff roll, the pilot noticed a decrease in manifold pressure in the right engine and felt a power reduction. He attempted to abort the takeoff with about 1,000 ft of runway pavement remaining. However, the airplane was traveling at 85 knots at the time of his decision, and the airplane would have needed about 2,400 ft of runway to stop. The airplane departed the runway surface, continued through a grassy area, and came to a stop in an adjacent field, which resulted in substantial damage to the nose and wing.

During the postaccident examination of the right engine, the engine was successfully test run, and no anomalies were found during the run that would have precluded normal operation or production of rated horsepower. The circumstances of the accident are consistent with the pilot choosing to abort the takeoff with inadequate runway distance remaining after a reported loss of engine power. The exact magneto timing was not determined, and although it could have affected the engine performance, the reason for the loss of engine power could not be determined based on the available evidence.

Probable Cause: The partial loss of right engine power for undetermined reasons with insufficient runway remaining for the aborted takeoff.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN15LA418
Status: Investigation completed
Duration: 4 years 1 month
Download report: Final report

Sources:

NTSB
FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=813CA

Location

Revision history:

Date/timeContributorUpdates
22-Sep-2015 16:02 Geno Added
21-Dec-2016 19:30 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
10-Nov-2019 14:30 ASN Update Bot Updated [Operator, Country, Nature, Departure airport, Destination airport, Source, Narrative, Accident report, ]
11-Nov-2019 17:44 harro Updated [Departure airport, Destination airport, Source, Narrative, Accident report, ]

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