ASN Wikibase Occurrence # 180194
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Date: | Monday 5 October 2015 |
Time: | 13:00 |
Type: | Cessna 152 |
Owner/operator: | Upper Limit Aviation |
Registration: | N6449M |
MSN: | 15284733 |
Year of manufacture: | 1980 |
Total airframe hrs: | 9715 hours |
Engine model: | Lycoming O-235 SERIES |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | SW of Cedar City Regional Airport (KCDC), Cedar City, UT -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Executive |
Departure airport: | Cedar City, UT (CDC) |
Destination airport: | Cedar City, UT (CDC) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A company chief pilot was performing a company check flight of a newly hired flight instructor. Data recovered from an on-board flight tracking system indicated that the airplane was maneuvering about 3,000 ft above ground level in the accident area; the final 35 seconds of data showed a near vertical descent toward the accident location. A witness saw the airplane descending vertically in a slight nose-down attitude "like a fluttering leaf." The airplane impacted the ground in a slightly nose-down and wings-level attitude, and ground impact marks around the airplane did not indicate any forward momentum. Examination of the airframe and engine found no abnormalities that would have precluded normal operation. The flight tracking data, the witness description, and the damage to the airplane are consistent with the airplane entering an aerodynamic stall and descending to ground impact. It could not be determined whether the stall was inadvertent or intentional (stall demonstration). Weight and balance calculations indicated that the airplane was about 40 pounds over maximum gross weight at takeoff and about 10 pounds over gross weight at the time of the accident; however, it is unlikely that this weight exceedance contributed to the loss of control.
Probable Cause: The failure of the pilots to maintain control of the airplane while maneuvering, which resulted in an aerodynamic stall from which they did not recover.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR16FA002 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N6449M Location
Revision history:
Date/time | Contributor | Updates |
05-Oct-2015 23:23 |
Geno |
Added |
05-Oct-2015 23:55 |
Geno |
Updated [Operator, Source, Damage, Narrative] |
06-Oct-2015 15:07 |
Geno |
Updated [Registration, Cn, Source] |
08-Oct-2015 11:28 |
Iceman29 |
Updated [Source] |
21-Dec-2016 19:30 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
26-Oct-2017 19:51 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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