Accident Cessna 175B Skylark N8115T,
ASN logo
ASN Wikibase Occurrence # 186135
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Saturday 2 April 2016
Time:17:07
Type:Silhouette image of generic C175 model; specific model in this crash may look slightly different    
Cessna 175B Skylark
Owner/operator:Private
Registration: N8115T
MSN: 17556815
Year of manufacture:1960
Total airframe hrs:2989 hours
Engine model:Teledyne Continental GO-300-D
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Jackson County, ENE of Hurley, MS -   United States of America
Phase: Landing
Nature:Private
Departure airport:Mobile, AL (MOB)
Destination airport:Slidell, LA (ASD)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The commercial pilot was flying the airplane on a cross-country flight, which was the first flight after the completion of an annual inspection. The pilot reported that he noted no anomalies during the preflight inspection or engine run-up. After takeoff, the airplane proceeded toward the destination airport between 1,200 and 1,500 ft mean sea level. After levelling off, the pilot slowly leaned the fuel-to-air ratio. The pilot added that, subsequently, the engine rpm "abruptly" decreased from 2,900 to 1,200. The pilot promptly pushed the mixture control to full rich, but this did not restore power. He then twice advanced the throttle, which briefly increased the engine power before it reduced to idle power again. He informed an air traffic controller of the problem, and the controller then provided the pilot with radar vectors to a nearby airport. However, after realizing the airplane would be unable to reach the airport, the pilot chose to execute a forced landing in a field, during which the nose landing gear separated from the airplane.

Examination of the engine compartment revealed that the mixture control in the cockpit was in the "full rich" position but that the mixture control lever at the carburetor was at the "idle cutoff" position. Movement of the mixture control in the cockpit resulted in the cable flexing rather than completely moving the mixture control lever at the carburetor, which was due to a plastic sheath that was covering a portion of the mixture control cable; the sheath prevented the cable from being properly secured and also prevented the full movement of the mixture control lever at the carburetor. The plastic sheath was not a part specified in the airplane's parts catalog.

During engine test-runs, the engine operated satisfactorily when the mixture control lever at the carburetor was in the "full-rich" position. Given that no other issues were identified during the postaccident test-run, it is likely that the plastic sheath's preventing the proper securing of the mixture control cable and full travel of the control at the carburetor led to the pilot's inability to properly control the mixture control lever at the carburetor and the subsequent partial loss of engine power. Although the mechanic who performed the last inspection indicated that he checked the mixture control for full travel and noted no discrepancies with the mixture control cable, he failed to detect the plastic sheath covering a portion of the mixture control cable, which prevented adequate securing of the cable.

Probable Cause: The mechanic's failure to identify and remove a plastic sheath covering a portion of the mixture control cable during an annual inspection, which prevented the proper securing of the mixture control cable and full travel of the control at the carburetor and subsequently led to the pilot's inability to properly control the mixture control lever at the carburetor and the resultant partial loss of engine power.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA16LA145
Status: Investigation completed
Duration: 3 years and 3 months
Download report: Final report

Sources:

NTSB
FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=8115T

Location

Revision history:

Date/timeContributorUpdates
03-Apr-2016 20:06 Geno Added
21-Dec-2016 19:30 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
06-Jul-2019 19:35 ASN Update Bot Updated [Operator, Nature, Departure airport, Destination airport, Source, Narrative, Accident report, ]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org