ASN Wikibase Occurrence # 186289
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Date: | Friday 8 April 2016 |
Time: | 15:02 |
Type: | Bellanca 7GCBC Citabria |
Owner/operator: | BIG Q AVIATION |
Registration: | N5046N |
MSN: | 1132-79 |
Year of manufacture: | 1979 |
Engine model: | Lycoming O-320-A2B |
Fatalities: | Fatalities: 1 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Mid-Way Regional Airport (KJWY), Midlothian/Waxahachie, TX -
United States of America
|
Phase: | Take off |
Nature: | Training |
Departure airport: | Midlothian, TX (JWY) |
Destination airport: | Midlothian, TX (JWY) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The flight instructor was demonstrating a takeoff to the student pilot in the tailwheel-equipped airplane. During the takeoff, the instructor was flying the airplane and was seated in the rear seat, with the student pilot observing and following along on the flight controls in the front seat. The instructor stated that, as the airplane lifted off the runway, he could not move the control stick. The airplane continued to climb in an increasingly nose-high pitch attitude, and the instructor stated that his efforts to apply forward pressure on the control stick had "no effect." The airplane subsequently experienced an aerodynamic stall and impacted the ground.
Examination of the airframe and engine revealed no preimpact anomalies that would have precluded normal operation, and examination of the flight controls found no evidence of interference. While the flight instructor expected the student pilot to follow along on the control stick, it could not be determined if the student interfered with the movement of the controls. With the instructor unable to move the elevator control and reduce the nose-high pitch attitude of the airplane, the airplane exceeded its critical angle of attack and experienced an aerodynamic stall.
Probable Cause: The flight instructor's inability to move the control stick after takeoff for undetermined reasons, which resulted in an exceedance of the airplane's critical angle of attack and inadvertent aerodynamic stall. The reason for the inability to move the control stick could not be determined, because postaccident examination revealed no evidence of flight control malfunctions or anomalies that would have precluded normal operation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN16FA145 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
History of this aircraft
Other occurrences involving this aircraft
4 March 1984 |
N5046N |
Ft. Eustis Flying Club |
0 |
Ft. Eustis, VA |
|
sub |
Location
Revision history:
Date/time | Contributor | Updates |
08-Apr-2016 22:30 |
Geno |
Added |
09-Apr-2016 00:11 |
Geno |
Updated [Aircraft type, Registration, Cn, Operator, Source, Narrative] |
11-Apr-2016 16:14 |
Geno |
Updated [Registration, Source, Narrative] |
15-Apr-2016 05:27 |
Anon. |
Updated [Total fatalities] |
21-Dec-2016 19:30 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
02-Jun-2017 05:49 |
PiperOnslaught |
Updated [Phase, Departure airport, Destination airport, Source, Narrative] |
19-Aug-2017 15:07 |
ASN Update Bot |
Updated [Operator, Other fatalities, Source, Narrative] |
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