Wirestrike Incident North American AT-6D N150U,
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ASN Wikibase Occurrence # 188257
 
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Date:Sunday 19 June 2016
Time:14:40
Type:Silhouette image of generic T6 model; specific model in this crash may look slightly different    
North American AT-6D
Owner/operator:Private
Registration: N150U
MSN: 88-14893
Year of manufacture:1942
Total airframe hrs:2939 hours
Engine model:P&W R-1340-AN-1
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Location:Cole County, east of Henley, MO -   United States of America
Phase: Manoeuvring (airshow, firefighting, ag.ops.)
Nature:Private
Departure airport:Jefferson City, MO (JEF)
Destination airport:Jefferson City, MO (JEF)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airline transport pilot reported that, about 30 minutes into the local flight, the engine experienced a total loss of power, and he conducted a forced landing to a powerline cut. He stated that the airplane was at low altitude at the time of the loss of engine power because he had been taking photos of a friend’s farm.
Two witnesses observed the airplane conducting aerobatic maneuvers during the flight. One of the witnesses stated that the airplane was flying so low that it startled her horses as it passed overhead. She then observed the airplane roll inverted; shortly thereafter, the engine became silent. The airplane lost altitude while still inverted and impacted trees. Examination of the wreckage revealed no preimpact mechanical malfunctions or anomalies that would have precluded normal operation. The airplane’s operating instructions stated that, “Inverted flying must be limited to 10 seconds because of engine difficulties resulting from prolonged inverted flight.” Because no anomalies were found during the examination, it is likely that the loss of engine power was a result of fuel disruption to the engine during the extended inverted flight.

Probable Cause: The pilot’s decision to conduct extended inverted flight, which resulted in a total loss of engine power due to fuel flow disruption. Contributing to the accident was his decision to conduct aerobatic maneuvers at low altitude, which precluded him from selecting a suitable landing site following the total loss of engine power.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN16LA222
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB
FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=150U
ex.USAAF/42-44629, N6983C.

Location

Revision history:

Date/timeContributorUpdates
20-Jun-2016 00:44 Geno Added
20-Jun-2016 17:20 Geno Updated [Aircraft type, Registration, Cn, Operator, Source]
21-Dec-2016 19:30 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
19-Aug-2017 16:43 ASN Update Bot Updated [Time, Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative]
08-Jul-2018 11:05 A.J. Scholten Updated [Cn, Source]

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