Accident Velocity TXL N916TC,
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ASN Wikibase Occurrence # 188822
 
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Date:Saturday 23 July 2016
Time:09:30
Type:Silhouette image of generic VELO model; specific model in this crash may look slightly different    
Velocity TXL
Owner/operator:Private
Registration: N916TC
MSN: 3RX177
Year of manufacture:2013
Total airframe hrs:161 hours
Engine model:Continental TSIO-550-C
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Sebastian Municipal Airport (X26), Sebastian, FL -   United States of America
Phase: Take off
Nature:Private
Departure airport:Sebastian, FL (X26)
Destination airport:Sebastian, FL (X26)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The commercial pilot stated that before departing on the personal flight, the engine did not start on the first attempt; he primed the engine, and then it started immediately. During the takeoff roll, he noted that he used more of the runway than usual. After rotation, the airplane was not climbing, and then the engine lost total power. He did not have time to restart the engine and performed a forced landing to a field, which resulted in substantial damage. An engine test run and an examination of the fuel pump were performed. The examination revealed that the aneroid adjustment within the fuel pump was set for too rich of a mixture. The rich mixture setting caused the engine to run normally until the manifold pressure went above 36 inches of pressure (in excess of the maximum manifold pressure for which the engine was certified); then it would stumble then lose power. After the aneroid adjustment was set for a leaner mixture, the fuel pump operated normally on the test bench without any anomalies. A review of maintenance work orders revealed that the fuel pump was removed, repaired, and reinstalled about 2 months before the accident. Given this information, it is likely that maintenance personnel set the aneroid adjustment too high at that time, which caused the engine to run with an excessively rich mixture, which resulted in a total loss of engine power on climbout.

Probable Cause: The total loss of engine power due to maintenance personnel’s improper setting of the aneroid adjustment.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA16LA268
Status: Investigation completed
Duration: 3 years and 9 months
Download report: Final report

Sources:

NTSB
FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N916TC

Location

Images:


Photo: FAA

Revision history:

Date/timeContributorUpdates
23-Jul-2016 18:30 Geno Added
25-Jul-2016 19:14 Geno Updated [Aircraft type, Registration, Cn, Operator, Phase, Departure airport, Source, Damage, Narrative]
19-Apr-2020 07:01 ASN Update Bot Updated [Time, Operator, Nature, Departure airport, Destination airport, Source, Narrative, Accident report, ]
19-Apr-2020 08:07 harro Updated [Source, Narrative, Photo, Accident report, ]

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