ASN Wikibase Occurrence # 19789
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Wednesday 23 April 2008 |
Time: | 10:00 |
Type: | Piper PA-28-140 Cherokee |
Owner/operator: | Private |
Registration: | N333KQ |
MSN: | 28-7325325 |
Year of manufacture: | 1973 |
Total airframe hrs: | 6420 hours |
Engine model: | Lycoming O-320 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Gilmer County Airport, Ellijay, Georgia -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | Elijay, GA (49A) |
Destination airport: | Atlanta, GA (PDK) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:After landing the airplane with the intent of obtaining fuel, the pilot learned that fuel services were not available at the airport and subsequently obtained 5 gallons of automotive fuel that he added to the left fuel tank. Following a pre-departure engine run-up, the takeoff proceeded normally until, about 200 feet above the ground when the engine began losing partial power, which was followed by a total power loss. The pilot attempted to troubleshoot the problem, and stated that he "switched [fuel] tanks" as the airplane descended. The airplane impacted trees about 2,000 feet from the runway and came to rest. Post-accident examination of the wreckage revealed that both fuel tanks remained intact. About 4.5 gallons of fuel were drained from the left fuel tank, and a trace amount of fuel was observed in the right fuel tank. The fuel selector valve was positioned to the right fuel tank position. A subsequent test run of the engine revealed that it started almost immediately and ran at low, intermediate, and high power settings. Examination of maintenance records revealed that the engine was last overhauled nearly 25 years prior to the accident flight.
Probable Cause: A loss of engine power for undetermined reasons.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC08LA167 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB
FAA register: 2. FAA:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=333KQ Location
Revision history:
Date/time | Contributor | Updates |
23-May-2008 02:43 |
Fusko |
Added |
03-Mar-2015 20:39 |
Dr. John Smith |
Updated [Operator, Departure airport, Destination airport, Source, Narrative] |
21-Dec-2016 19:14 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:16 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:20 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
03-Dec-2017 10:42 |
ASN Update Bot |
Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation