ASN Wikibase Occurrence # 198974
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Date: | Monday 19 September 2016 |
Time: | 17:00 |
Type: | Piper PA-32R-300 |
Owner/operator: | Private |
Registration: | N4477F |
MSN: | 32R-7680449 |
Year of manufacture: | 1976 |
Total airframe hrs: | 5101 hours |
Engine model: | Lycoming IO-540-KIG50 |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Grants, NM -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Grants, NM (GNT) |
Destination airport: | Cedar City, UT (CDC) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:After a preflight inspection and engine run up that revealed no anomalies, the private pilot and two passengers were departing on a cross-country flight. The pilot stated that the airplane became airborne approximately 5,000 ft down the 7,172-ft-long runway at 80 knots. Approximately 100 feet above ground level, he heard a "gurgle" and the engine experienced a loss of power. The pilot verified that the fuel pump was on and the throttle was in its full-forward position. The pilot then located a forced landing site and during the landing, the airplane impacted a tree. The occupants egressed, and the airplane was subsequently consumed by postcrash fire. The accident airport was located at an elevation about 6,500 ft mean sea level (msl). Given the atmospheric conditions at the time of the accident, the density altitude exceeded 9,000 ft msl, which would have significantly increased the airplane's takeoff distance and reduced its climb capability. The pilot's experience operating in high density altitude environments could not be determined. Review of photos from the accident site revealed that the fuel selector handle appeared to be located between the left fuel tank and off positions; however, the fuel selector was not examined and its position could not be verified, therefore, the reason for the reported loss of engine power could not be determined.
Probable Cause: A loss of engine power for reasons that could not be determined based on the available information.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN16LA375 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
19-Aug-2017 16:16 |
ASN Update Bot |
Added |
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