ASN Wikibase Occurrence # 200199
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 20 June 2017 |
Time: | 17:00 |
Type: | Bellanca 7GCBC |
Owner/operator: | Private |
Registration: | N88237 |
MSN: | 744-74 |
Year of manufacture: | 1974 |
Total airframe hrs: | 1390 hours |
Engine model: | Lycoming O-320 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Edgewood, NM -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Edgewood, NM (1N1) |
Destination airport: | Edgewood, NM (1N1) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that, about 8 seconds into the takeoff roll in gusting wind conditions at highdensity altitude, the airplane “suddenly and expectantly lifted off the runway in a steep angle of attack.” He added that he immediately reduced power to idle to abort the initial climb, and the airplane “settled back onto the runway but landed hard.” He further added that, during the landing roll, he lost directional control, and the airplane veered off the runway, coming to rest in the dirt alongside the runway.
The fuselage, left wing, and aileron sustained substantial damage.
The pilot reported that there were no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation.
An automated weather observation station, 10 nautical miles southeast of the accident airport, reported that, 5 minutes before the accident, the wind was from 150° at 16 knots, gusting to 25 knots. The pilot reported that he observed the wind from 300° at 8 knots, gusting to 15 knots. He reported that the takeoff was on runway 9. He further reported that the density altitude was 10,000 ft at the departure airport.
Probable Cause: The pilot's decision to take off with a gusting tailwind, which resulted in a loss of pitch control during the initial climb and a subsequent hard landing and loss of directional control.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | GAA17CA357 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
04-Oct-2017 17:40 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation