ASN Wikibase Occurrence # 200910
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Date: | Friday 28 April 2017 |
Time: | 15:06 |
Type: | Mooney M20J |
Owner/operator: | Private |
Registration: | N1157N |
MSN: | 24-1288 |
Year of manufacture: | 1982 |
Total airframe hrs: | 2254 hours |
Engine model: | Lycoming IO-360-A3B6D |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Cedar Key, FL -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Ocala, FL (KCDK) |
Destination airport: | Cedar Key, FL (CDK) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot reported that, during the landing roll, he had traveled about halfway down the 2,355 ft-long runway when he realized that a go-around was going to be required. He could not recall the airplane’s airspeed when the airplane touched down on the runway that was located steps from the ocean. However, he did recall that he initiated the go-around by applying full throttle, retracting the flaps to 0, and rotating at 62 knots. The airplane “lifted off but did not gain altitude.” The pilot lowered the nose to accelerate, but the airplane stalled and impacted the water. The airplane sustained substantial damage to the right wing spar and aileron.
According to the manufacturer’s Pilot’s Operating Handbook, the go-around procedure is:
CAUTION
To minimize control wheel forces during go-around, timely nose-down trimming is recommended to counteract nose up pitching moment as power is increased and/or flap retraction.
Power…..Full Throttle/2700 RPM
Mixture…..Full Rich
Airspeed…..65 KIAS
Wing Flaps…..Takeoff position after climb established
Trim…..Nose Down (to reduce control forces)
Airspeed…..Accelerate to 76 KIAS
Landing Gear…..-Retract
Wing Flaps…..Retract
Cowl Flaps…..Open
Airspeed…..Accelerate to 86 KIAS
The pilot reported that there were no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation.
Probable Cause: The pilot’s failure to follow the manufacturer’s go-around procedure, which resulted in an aerodynamic stall.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | GAA17CA211 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
05-Nov-2017 08:46 |
ASN Update Bot |
Added |
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