Accident Bell 47G-3B1 N32PH,
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ASN Wikibase Occurrence # 202130
 
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Date:Monday 19 April 1999
Time:07:30 LT
Type:Silhouette image of generic B47G model; specific model in this crash may look slightly different    
Bell 47G-3B1
Owner/operator:Provine Helicopter Service, In
Registration: N32PH
MSN: 2768
Year of manufacture:1962
Total airframe hrs:12767 hours
Engine model:Allison 250-C-20B
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Thomastown, MS -   United States of America
Phase: Unknown
Nature:Agricultural
Departure airport:
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot stated he was pulling up the aerial spray rigged helicopter from the platform of the 'nurse truck' in order to reposition for a better placement on the platform, when he experienced uncommanded rotation. His ground crew stated, as he pulled up, a piece of the aircraft flew off and the tail rotor began to spin down. The aircraft went into an uncontrollable rotation, and the main rotor blades collided with an adjacent small tree stand. The helicopter impacted the terrain, the right landing skid collapsed, and the helicopter rolled over on its right side. Subsequent examination of the wreckage and interviews of the pilot, passenger, and ground crew revealed the approach and pull up for the second approach were into downwind conditions. The piece of the aircraft that flew off was a section of the tail rotor drive shaft. Except for the missing piece of shaft, no mechanical abnormalities could be found in the pilot controls, engine, or drive train.

Probable Cause: An in-flight loss of control caused by the main rotor severing the tail rotor drive shaft as a result of the pilot's cyclic pull-up into a tailwind for his second approach and landing. The loss of the tail rotor caused an uncontrollable descent and tree strike with the main rotor and in-flight collision with terrain. Contributing to the accident was the pilot's improper decision to make a downwind approach and landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA99LA133
Status: Investigation completed
Duration: 11 months
Download report: Final report

Sources:

NTSB MIA99LA133

Revision history:

Date/timeContributorUpdates
26-Nov-2017 12:40 ASN Update Bot Added
08-Apr-2024 06:57 ASN Update Bot Updated [Time, Aircraft type, Other fatalities, Source, Narrative, Accident report]

Corrections or additions? ... Edit this accident description

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