ASN Wikibase Occurrence # 20535
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Date: | Monday 2 June 2008 |
Time: | 08:15 |
Type: | Schweizer 269C (300C) |
Owner/operator: | High Desert Helicopters, LLC |
Registration: | N1510A |
MSN: | S-1886 |
Engine model: | Textron Lycoming HIO-360-D1A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | near Pleasant View, UT -
United States of America
|
Phase: | Approach |
Nature: | Training |
Departure airport: | Ogden, UT (KOGD) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The instructor pilot and the private pilot under instruction arrived at the location where they were going to practice pinnacle approaches and landings. They reconnoitered the area at 300 feet above ground level (agl) in preparation for landing. They performed a power check at 500 feet agl, and concluded that engine power was sufficient to maintain an out of ground effect hover. The student began the approach at 350 feet agl. The helicopter's rate of descent was 500 feet per minute (fpm) at 25 knots of airspeed. Settling with power (vortex ring state) can be encountered when rates of descent are greater than 300 feet per minute and airspeed below that of translational lift. The helicopter began to overshoot the point of intended landing, and the approach became almost vertical. At 30 feet agl, the helicopter's descent rate increased and the student aborted the approach and began a go-around. The instructor realized that rotor revolutions-per-minute (rpm) had degraded below the normal range, so he took the control of the helicopter. Because the go-around had been initiated, the helicopter was moving forward slowly over a descending slope and the instructor was not able to land the helicopter. He attempted to gain power by lowering and raising collective; however, the helicopter's skid contacted the ground and the helicopter rolled over.
Probable Cause: The pilot under instruction's encounter with a settling with power condition, and the flight instructor's failure to maintain adequate rotor rpm during the subsequent go-around. Also causal was the instructor pilot's delayed remedial action during the approach sequence and his inadequate supervision of the flight.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX08CA138 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
03-Jun-2008 23:03 |
Fusko |
Added |
21-Dec-2016 19:14 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:16 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:20 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
03-Dec-2017 11:21 |
ASN Update Bot |
Updated [Cn, Operator, Other fatalities, Departure airport, Source, Narrative] |
21-Sep-2019 15:56 |
BEAVERSPOTTER |
Updated [Cn, Damage] |
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