ASN Wikibase Occurrence # 207170
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Date: | Tuesday 6 March 2018 |
Time: | 21:17 |
Type: | Cirrus SR20 |
Owner/operator: | Private |
Registration: | N101AD |
MSN: | 1198 |
Year of manufacture: | 2002 |
Total airframe hrs: | 1912 hours |
Engine model: | Continental IO-360 SER |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Harford County Airport (0W3), Churchville, MD -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Calhoun, GA (CZL) |
Destination airport: | Mount Holly, NJ (VAY) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot stated that, before departure for a cross-country, personal flight at night in visual conditions, he checked the weather using several online weather resources, which showed that the destination airport was reporting visual meteorological conditions. He reported that, about 30 minutes before the anticipated arrival at the destination airport, it started snowing. He descended the airplane to get out of the snow, but the airplane encountered a temperature inversion, and because snow was accumulating on the wings, the pilot chose to divert to the closest airport. He approached the runway at a higher-than-normal speed, and the airplane ballooned during touchdown and then drifted off the side of the runway. He attempted a go-around, but the airplane could not gain enough airspeed to become airborne, and it subsequently impacted two trucks, which resulted in substantial damage to the airframe.
The pilot reported that there were no mechanical malfunctions or failures with the airplane that would have precluded normal operation. It is likely that the pilot’s improper landing flare resulted in the airplane ballooning upon landing and led to his subsequent loss of directional control.
Probable Cause: The pilot's improper landing flare, which resulted in the airplane ballooning on touchdown, and his subsequent failure to maintain directional control during the attempted landing and subsequent go-around.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA18LA098 |
Status: | Investigation completed |
Duration: | 1 year and 8 months |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N101AD Location
Revision history:
Date/time | Contributor | Updates |
07-Mar-2018 18:18 |
Geno |
Added |
07-Mar-2018 21:07 |
Geno |
Updated [Aircraft type, Registration, Cn, Operator, Location, Destination airport, Source, Narrative] |
11-Nov-2019 17:42 |
ASN Update Bot |
Updated [Time, Operator, Total occupants, Nature, Departure airport, Destination airport, Source, Narrative, Accident report, ] |
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