ASN Wikibase Occurrence # 20792
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Date: | Sunday 1 June 2008 |
Time: | 08:16 |
Type: | Lightning |
Owner/operator: | Private |
Registration: | N62JV |
MSN: | 7 |
Engine model: | Jabaru 3300 |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Marana, AZ -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | Tucson, AZ (KRYN) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:While maneuvering adjacent to a private airstrip at a low altitude, witnesses reported observing the propeller assembly separate from the airplane. The pilot maneuvered towards the airstrip and leveled out on runway heading about mid-length of the runway. As the airplane crossed over the end of the runway, it banked to the left and descended into terrain, impacting an open desert field adjacent to several residential homes. Examination of the airplane revealed that the airframe and both wings were structurally damaged. The propeller assembly, including the propeller flange extension were found separated from the engine crankshaft. No further anomalies were noted with the airframe and engine that would have precluded normal operation. The attachment bolts were installed on a painted surface of the propeller flange extension. The paint surrounding this area was flaking away from the surface. Evidence of thread locking material was observed in the threaded areas consistent with installation instructions. Examination of the attachment bolts revealed that four of the six bolts exhibited fracture surfaces consistent with fatigue. One of the four bolts exhibited a multifaceted fracture surface with multiple origins around the circumference. Hardness of this bolt was checked and found to be within the specified hardness range.
Probable Cause: The insufficient clamping force resulting in a fatigue fracture of the propeller extension attachment bolts and subsequent separation of the propeller assembly in flight. Contributing to the accident was the pilot's failure to maintain sufficient airspeed to avoid an inadvertent stall while maneuvering during the emergency approach to the airport.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA08LA149 |
Status: | Investigation completed |
Duration: | 6 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
07-Jun-2008 23:33 |
Fusko |
Added |
21-Dec-2016 19:14 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:16 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:20 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
01-Mar-2017 07:20 |
PiperOnslaught |
Updated [Phase, Departure airport, Source, Narrative] |
03-Dec-2017 11:23 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Source, Narrative, Plane category] |
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