Loss of control Accident Taylorcraft BC12-D N94909,
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ASN Wikibase Occurrence # 211295
 
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Date:Monday 21 May 2018
Time:19:10
Type:Silhouette image of generic TAYB model; specific model in this crash may look slightly different    
Taylorcraft BC12-D
Owner/operator:Private
Registration: N94909
MSN: 9309
Year of manufacture:1946
Engine model:Continental A65
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Doug Bolton Field Airport (02GA), Commerce, GA -   United States of America
Phase: Initial climb
Nature:Private
Departure airport:Commerce, GA (N/A)
Destination airport:Commerce, GA (N/A)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The commercial pilot departed on a visual flight rules local flight. A witness saw the pilot conduct a preflight inspection of the accident airplane and depart on a 10-minute flight. When the airplane returned to the airstrip to land, the witness heard the engine rpm "going up and down." After the airplane landed, the pilot began taxiing toward the hangar but then taxied back to the runway for another takeoff. The witness stated that the airplane reached an altitude between about 50 and 75 ft above the runway with the engine sputtering. At that time, the airplane seemed to slow and was just above the trees when the right wing and then the nose dropped, which was followed by an impact with trees.

Postaccident examination of the engine revealed no evidence of any preimpact mechanical malfunctions or failures that would have precluded normal operation. The weather conditions near the accident site at the time of the accident were conducive to the formation of serious carburetor icing at descent engine power settings. Given that these conditions existed, and that the witness reported the engine rpm may have been fluctuating during the airplane's previous landing approach, it is likely that carburetor ice accumulated during the prior descent and possibly the taxi period that followed prior to the accident takeoff. The undetected partial loss of power during the accident takeoff ultimately led to an aerodynamic stall from which the pilot was unable to recover.

Probable Cause: The pilot's failure to effectively mitigate an accumulation of carburetor ice, which resulted in an undetected partial loss of engine power and an aerodynamic stall during takeoff.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA18FA149
Status: Investigation completed
Duration: 1 year and 11 months
Download report: Final report

Sources:

NTSB

FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=94909

Location

Revision history:

Date/timeContributorUpdates
22-May-2018 05:14 Geno Added
22-May-2018 05:16 Geno Updated [Source]
22-May-2018 16:52 Geno Updated [Time, Aircraft type, Registration, Cn, Operator, Source, Damage, Narrative]
22-May-2018 17:16 Geno Updated [Registration, Total fatalities, Source, Narrative]
22-Apr-2020 17:05 ASN Update Bot Updated [Time, Operator, Nature, Departure airport, Destination airport, Source, Narrative, Accident report, ]

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