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ASN Wikibase Occurrence # 213579
Last updated: 15 October 2021
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Date:23-DEC-2016
Time:11:45
Type:Silhouette image of generic P28A model; specific model in this crash may look slightly different
Piper PA-28-161
Owner/operator:PC Air Ventures Ltd.
Registration: N31202
MSN: 28-7816552
Fatalities:Fatalities: 1 / Occupants: 1
Other fatalities:0
Aircraft damage: Substantial
Category:Accident
Location:Middlebury, VT -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Middlebury, VT (6B0)
Destination airport:Middlebury, VT (6B0)
Investigating agency: NTSB
Narrative:
The airplane had not been flown recently, and, before the personal flight, the private pilot cleared snow from the airplane's wings, charged the airplane's battery, and preheated the engine. He then performed a preflight inspection and drained the fuel tanks. The pilot taxied the airplane to the runway and departed. A witness reported that, during the initial climb, the airplane's wings "wagged," then the engine "skipped" and then "went back to normal." Another witness reported that he heard the engine "sputtering" and saw the airplane make a 180 turn back toward the runway. Both witnesses stated that the airplane then quickly descended. The observations of the witnesses are consistent with the pilot losing control of the airplane while attempting to return to the runway following a partial or complete loss of engine power.

Examination of the airframe and engine revealed no anomalies that would have precluded normal operation with the exception of the right fuel cap, which remained seated but its gasket exhibited cracking. Although there was no contamination noted in the fuel system during the engine examination, it is possible that water had leaked through the cracked fuel cap gasket and was not completely drained during the pilot's preflight inspection. Then, following the wings being "wagged," the remaining water entered the fuel system and resulted in a partial or total loss of engine power. In response to the power loss, the pilot attempted to return to the runway; however, during the turn, the pilot failed to maintain sufficient airspeed, which resulted in the airplane exceeding its critical angle of attack and entering an aerodynamic stall. The pilot's decision to return to the runway was contrary to FAA guidance that recommended continuing straight ahead following an engine failure on takeoff.

The pilot did not hold a medical certificate and had a history of seizures. However, it is unlikely that the pilot had a seizure at the time of the accident as he was taking the medication levetiracetam to prevent seizures, and a seizure would have led to sudden incapacitation, which is inconsistent with the witness observations that indicate an intentional return to the airport. The pilot had been maintained on levetiracetam since 2010 without a complaint about somnolence; therefore, it is unlikely his use of this medication contributed to the accident. Tramadol was identified only in the pilot's urine, which indicated it was used many hours to days before the accident and was no longer present at impairing levels at the time of the accident. Overall, there was no evidence of a medical condition or medication that contributed to the circumstances of this accident.

Probable Cause: The pilot's improper decision to return to the airport following a partial or complete loss of engine power during takeoff initial climb and his failure to maintain sufficient airspeed while maneuvering, which resulted in exceedance of the critical angle of attack and an aerodynamic stall.

Sources:

NTSB

Accident investigation:
cover
  
Investigating agency: NTSB
Status: Investigation completed
Duration: 1 year and 7 months
Download report: Final report
Location


Revision history:

Date/timeContributorUpdates
22-Jul-2018 18:50 ASN Update Bot Added

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