Accident Cessna 140 N89093,
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ASN Wikibase Occurrence # 214454
 
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Date:Tuesday 14 August 2018
Time:10:30 LT
Type:Silhouette image of generic C140 model; specific model in this crash may look slightly different    
Cessna 140
Owner/operator:Private
Registration: N89093
MSN: 8097
Year of manufacture:1946
Total airframe hrs:2244 hours
Engine model:Continental C85-12
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Snake River at Sunrise Skypark Airport (ID40), Marsing, ID -   United States of America
Phase: Landing
Nature:Private
Departure airport:Nampa, ID
Destination airport:Nampa, ID
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
During a low pass over the runway, the pilot advanced the throttle, but the engine failed to respond. After switching fuel tanks, the pilot initiated a forced landing to a shallow part of a river that paralleled the runway. The airplane came to rest upright in the river, partially submerged, and sustained substantial damage to the lower fuselage and firewall.

Postaccident examination of the airplane revealed that the engine initially would not run. The carburetor was removed, partially disassembled, and examined. Evidence of corrosion was observed in the float bowl. The carburetor bowl was cleaned internally, reassembled, and reinstalled on the engine. Additional attempts to run the engine revealed that the engine would not run at power settings below 1,300 rpm.

Subsequent examination of the carburetor revealed that the throttle shaft was loose in its bushings or mounting to the casting. When the carburetor was installed on a fuel flow bench, immediate leaks were noted audibly, one at the throttle shaft seals and one in the area of the accelerator pump. Indications of blockage in the idle chambers of the carburetor were present, and at idle ranges, the fuel flows were significantly out of specification which likely led to the loss of engine power. Removal of the idle tube showed significant corrosion and contaminants in that area. The source of contaminants was not determined.

Probable Cause: The loss of engine power during a low pass as a result of a blockage of the carburetor idle chambers which led to a forced landing in a river.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR18LA224
Status: Investigation completed
Duration: 3 years
Download report: Final report

Sources:

NTSB WPR18LA224

FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=89093

Location

Revision history:

Date/timeContributorUpdates
16-Aug-2018 05:21 Geno Added
09-Jul-2022 05:20 ASN Update Bot Updated [Time, Total occupants, Other fatalities, Nature, Departure airport, Destination airport, Source, Damage, Narrative, Category, Accident report]

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