Accident Beechcraft 95 Travel Air N2733Y,
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ASN Wikibase Occurrence # 217207
 
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Date:Friday 24 January 2003
Time:16:26
Type:Silhouette image of generic BE95 model; specific model in this crash may look slightly different    
Beechcraft 95 Travel Air
Owner/operator:Private
Registration: N2733Y
MSN: TD-72
Total airframe hrs:9679 hours
Engine model:Lycoming O-360-A1A
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Destroyed
Category:Accident
Location:Rancho Cucamong, CA -   United States of America
Phase: En route
Nature:Private
Departure airport:Upland-Cable Airport, CA (CCB/KCCB)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
While in cruise flight, a portion of a propeller blade separated from the right engine. The resulting vibration partially separated the engine from its airframe mounts, and the uncontrollable airplane rolled inverted and dived into a private residence. The house was severely damaged, the airplane was destroyed. The separated propeller was overhauled about 3 years and 5 operational hours prior to the accident flight. The separated 2.5-foot-long span of the failed blade was found about 1 mile from the main wreckage. The blade was examined by the NTSB's Metallurgical Laboratory, which found that the blade failed as a result of fatigue cracking initiated by corrosion pitting in the pilot tube bore. A fatigue crack had initiated at two corrosion pit sites in the bore, which had been painted over without the corrosion being dressed out during the overhaul. Also, many additional corrosion pits were located circumferentially in line with the origin area. The blade's bore was also contaminated with glass beads. All of these conditions found during the examination were contrary to the procedural steps in the manufacturer's overhaul instructions, and established that the blade was reassembled with an incomplete and improper overhaul. The FAA inspector assigned to oversee the overhaul company said he did not observe any repair station deficiencies during his surveillance inspections. A Safety Board inspection following the accident disclosed that the repair station's personnel were not following prescribed manufacturer overhaul procedures, did not have the required chemicals for blade treatment, and did not possess required procedure manuals. Additional inspections of other propellers overhauled by the company revealed that propellers overhauled as early as 1997, when the company commenced business, showed evidence of corrosion in the pilot bores, and were unairworthy.

Probable Cause: The fracture and separation of a propeller blade during cruise flight due to fatigue and corrosion pits in the blade pilot bore, and an improper overhaul of the separated propeller by repair station personnel. Factors contributing to the accident were the FAA's inadequate surveillance of the repair station, and the repair station's inadequate procedures.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX03FA074
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20030206X00174&key=1

Location

Revision history:

Date/timeContributorUpdates
03-Nov-2018 20:40 ASN Update Bot Added
06-Jun-2023 10:47 Ron Averes Updated

Corrections or additions? ... Edit this accident description

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