ASN Wikibase Occurrence # 21761
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Date: | Wednesday 16 July 2008 |
Time: | 10:15 |
Type: | Cessna 441 Conquest II |
Owner/operator: | Private |
Registration: | N441HK |
MSN: | 441-0336 |
Year of manufacture: | 1985 |
Total airframe hrs: | 5643 hours |
Engine model: | Garrett TPE-331-10N |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Sunriver Airport, Sunriver, OR -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Bakersfield, CA (KBFL) |
Destination airport: | Sunriver, OR (S21) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was executing a day visual flight rules full-stop landing and touched down on the main landing gear near the approach end of the runway. Soon after the initial touchdown, the airplane became airborne again. Instead of initiating a go-around, the pilot attempted to continue the landing sequence. During that attempt, the airplane bounced on the runway three or four times, each time the rebound back into the air and the runway contact was more severe. During the last contact the airplane impacted the runway with sufficient force to result in the failure of the right main landing gear actuator rod, and in the right propeller contacting the runway surface multiple times. The pilot then initiated a go-around, but since the right engine had failed due to the multiple propeller strikes, the airplane produced asymmetrical thrust and began to roll to the right, veering off the right side of the runway. Soon thereafter its right wing collided with a tree and the airplane impacted terrain in an open field. The airplane was consumed by fire shortly after the collision. Postcrash inspection found no evidence of mechanical failure or malfunction with the airframe or either engine.
Probable Cause: The pilot's misjudged landing flare and improper recovery from a bounced landing, and the pilot's failure to maintain directional control during the go-around after one of the airplane's propellers struck the runway.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA08FA161 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Images:
In happier times: 12-14-2006 KBFL, Bakersfield, CA
Revision history:
Date/time | Contributor | Updates |
17-Jul-2008 10:28 |
Fusko |
Added |
17-Jul-2008 21:27 |
Anon. |
Updated |
19-Jul-2008 02:12 |
harro |
Updated |
23-Jul-2008 23:22 |
Fusko |
Updated |
19-Mar-2012 23:12 |
Anon. |
Updated [Source] |
21-Dec-2016 19:14 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:16 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:20 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
22-Nov-2017 10:44 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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