ASN Wikibase Occurrence # 21827
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Date: | Friday 4 July 2008 |
Time: | 16:00 |
Type: | Cessna 150J |
Owner/operator: | Sky Ads |
Registration: | N60486 |
MSN: | 15070346 |
Year of manufacture: | 1969 |
Engine model: | Lycoming O-360 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Seal Beach, CA -
United States of America
|
Phase: | En route |
Nature: | Banner and glider towing |
Departure airport: | Compton, CA (CPM) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that he was towing a banner along the ocean shoreline at an altitude of 500 feet and an airspeed of 40 mph when the engine lost power. He dropped the banner into the water, but was unsuccessful in attempting to restart the engine. The pilot ditched the airplane in the ocean about 100 feet from shore. A Federal Aviation Administration inspector examined the airplane after it was pulled onto the beach. The inspector reported that the right wing sustained structural damage. Additionally, the inspector noted that the airplane had been modified extensively, and one of the modifications included replacement of the original two position (ON/OFF) fuel selector valve with a four position fuel selector valve (BOTH ON/LEFT/RIGHT/OFF). The fuel selector valve was found in the LEFT tank position. The left tank contained about 1 gallon of fuel, and the right tank was full of fuel. The pilot stated that he was aware the airplane had been extensively modified, but was not aware that the fuel selector valve had been changed. He further stated that he had never touched the fuel selector switch, as he thought it was ON or OFF only. The operator reported that the pilot had received training in the airplane that included use of the four position fuel selector valve.
Probable Cause: Fuel starvation due to the pilot's improper fuel management procedures and failure to select a tank containing fuel. Contributing to the accident was the lack of suitable terrain for the forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX08CA215 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
24-Jul-2008 11:33 |
Fusko |
Added |
21-Dec-2016 19:14 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:16 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:20 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
03-Dec-2017 11:26 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Source, Narrative] |
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