ASN Wikibase Occurrence # 223181
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Date: | Sunday 17 March 2019 |
Time: | 15:05 LT |
Type: | Hughes 369HS |
Owner/operator: | Private |
Registration: | N119T |
MSN: | 760844S |
Year of manufacture: | 1976 |
Engine model: | Rolls-Royce C-18/T63-700 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | College Street, Newberg, OR -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Beaverton, OR |
Destination airport: | McMinnville Municipal Airport, OR (KMMV) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot and his passenger were enroute to an airport to refuel when the engine lost all power. The pilot performed a forced landing in an open field, during which the helicopter landed hard and rolled over. No fuel was found inside the helicopter's fuel tank following the accident. During an engine test run, the engine started normally and operated through all power settings with no evidence of a mechanical anomaly.
The helicopter was fueled to capacity about two weeks before the accident and, at the time of the accident, had flown a total of about 2 hours, 44 minutes since it was fueled. The pilot reported that the helicopter's fuel consumption rate was between 14 and 16 gallons per hour (gph); however, the owner's manual performance charts indicated a consumption of 21 gph, and during the postaccident test run, the engine consumed about 26 gph at approximate cruise power demands. At these fuel consumption rates, the helicopter's fuel endurance with full fuel was between 2 hours, 35 minutes, and 2 hours, 54 minutes. It is likely that the pilot miscalculated the amount of fuel needed for the flight using incorrect fuel consumption rates, which resulted in fuel exhaustion and a subsequent total loss of engine power.
Probable Cause: The pilot's improper fuel planning, which resulted in fuel exhaustion and a subsequent total loss of engine power.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR19LA097 |
Status: | Investigation completed |
Duration: | 3 years 1 month |
Download report: | Final report |
|
Sources:
NTSB WPR19LA097
FAA register:
https://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=119T Location
Revision history:
Date/time | Contributor | Updates |
18-Mar-2019 12:51 |
gerard57 |
Added |
18-Mar-2019 15:20 |
RobertMB |
Updated [Aircraft type, Total occupants, Location, Departure airport, Destination airport, Source] |
18-Mar-2019 15:29 |
RobertMB |
Updated [Aircraft type, Registration, Cn, Location, Destination airport, Source, Narrative] |
18-Mar-2019 15:42 |
Geno |
Updated [Phase, Departure airport, Destination airport, Source, Narrative] |
02-Jul-2022 14:13 |
ASN Update Bot |
Updated [Time, Other fatalities, Source, Narrative, Category, Accident report] |
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