ASN Wikibase Occurrence # 22791
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Date: | Wednesday 10 September 2008 |
Time: | 13:50 |
Type: | Cessna T210N Centurion |
Owner/operator: | Air Flight Service |
Registration: | N6278C |
MSN: | 21063853 |
Year of manufacture: | 1979 |
Total airframe hrs: | 8147 hours |
Engine model: | Continental TSIO-520 SER |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | San Francisco Bay, Oakland, CA -
United States of America
|
Phase: | En route |
Nature: | Executive |
Departure airport: | San Jose, CA (RHV) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During a local photo flight at an altitude of 1,500 feet mean sea level (msl), the pilot reported a decrease in engine power followed by a complete loss of engine oil pressure. The pilot determined that due to his location and altitude, he was forced to make a landing on the water. During the landing, the airplane sustained substantial damage to the horizontal stabilizers and to the bottom of the fuselage. During the post-accident investigation, it was determined that the number two and three cylinders had been replaced 137.1 flight hours prior to the accident. During the engine examinations, thermal discoloration of the crankshaft main journals and damage to various other internal components were noted. The crankshaft was fractured just forward of the number two main bearing. The fracture surfaces of the crankshaft were mechanically damaged due to rotational forces. The number two main bearings were not found in the main bearing support diameters. Several bearing fragments were found in the oil sump and on the bearing support diameter. The crankcase itself had been compromised just above the number one cylinder. A review of the maintenance logbooks noted that the engine was beyond manufacturers' recommendations for time between overhaul. Several maintenance discrepancies and non-compliance with manufacturers' recommendations were also noted.
Probable Cause: A loss of engine power while maneuvering due to the disintegration of the number two main bearing, which resulted in a fracture of the crankshaft. Contributing to the accident was inadequate maintenance.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX08LA292 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
11-Sep-2008 10:54 |
jorgetadeu7 |
Added |
21-Dec-2016 19:14 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:16 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:20 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
03-Dec-2017 12:05 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Source, Narrative] |
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