ASN Wikibase Occurrence # 27285
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Date: | Wednesday 10 April 2002 |
Time: | 16:25 |
Type: | Beechcraft E18S |
Owner/operator: | Charles T. Madsen |
Registration: | N686Q |
MSN: | BA-400 |
Year of manufacture: | 1959 |
Engine model: | Pratt & Whitney R-985-AN-14B |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Juneau, AK -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Juneau, AK (JUN) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Information verified through data from accident investigation authorities |
Narrative:The certificated airline transport pilot was departing on a 14 CFR Part 91 personal flight. The purpose of the flight was to deliver a load of wooden roofing shakes to a friend's remote lodge. Witnesses reported that just after takeoff, as the airplane climbed to about 200 to 300 feet above the ground, the airplane abruptly pitched up about 70 degrees, and drifted to the right. The airplane continued to turn to the right as the nose of the airplane lowered momentarily. As the airplane flew very slowly the landing gear was extended. The nose of the airplane pitched up again, the right wing dropped, and the airplane descended. One witness described the descent as: "The wings rocked back and forth as it descended, like a card in the wind, with the nose of the airplane slightly higher." The airplane impacted shallow water in an area of tidal mud flats. A postaccident investigation revealed that the estimated gross weight of the airplane at takeoff was 11,500.8 pounds, 1,400.8 pounds in excess of the airplane's maximum takeoff gross weight. The airplane's center of gravity could not be calculated due to the fact that the exact location/station of the cargo could not be determined. Examination of the airplane revealed no evidence of any preimpact mechanical anomalies.
Probable Cause: The pilot's excessive loading of the airplane that precipitated an inadvertent stall/mush during the initial climb.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ANC02FA028 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20020419X00557&key=1 Location
Revision history:
Date/time | Contributor | Updates |
27-Sep-2008 01:00 |
ASN archive |
Added |
21-Dec-2016 19:14 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:16 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
21-Dec-2016 19:20 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
09-Dec-2017 16:06 |
ASN Update Bot |
Updated [Cn, Operator, Nature, Departure airport, Source, Narrative] |
16-Oct-2018 07:59 |
TB |
Updated [Aircraft type, Narrative] |
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