Accident Beechcraft 58 Baron N158WB,
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ASN Wikibase Occurrence # 35156
 
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Date:Sunday 25 April 1993
Time:18:38 LT
Type:Silhouette image of generic BE58 model; specific model in this crash may look slightly different    
Beechcraft 58 Baron
Owner/operator:Jay M. Supkoff
Registration: N158WB
MSN: TH-396
Year of manufacture:1973
Total airframe hrs:2310 hours
Engine model:CONTINENTAL IO-520-C
Fatalities:Fatalities: 2 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Tucson, AZ -   United States of America
Phase: Initial climb
Nature:Private
Departure airport:
Destination airport:San Jose, CA (KSJC)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
THE PILOT HAD RECENTLY PURCHASED THE TWIN ENGINE AIRPLANE AND HAD ACCUMULATED ABOUT 123 TOTAL HOURS OF MULTI ENGINE TIME, WITH ABOUT 115 HOURS IN THE ACCIDENT AIRPLANE. WITNESSES STATED THAT JUST AFTER ROTATION THE AIRPLANE PITCHED UP ABRUPTLY AND ROTATED TO THE RIGHT IMPACTING THE GROUND ABOUT 2000 FEET BEYOND THE APPROXIMATE POINT OF ROTATION AND ABOUT 1500 FEET TO THE RIGHT OF THE RUNWAY CENTER LINE. POST CRASH EXAMINATION OF THE WRECKAGE REVEALED THAT THE AFT UTILITY DOORS WERE UNLATCHED, WITH THE AFT DOOR ROTATED REARWARD AGAINST THE FUSELAGE AND THE EXTENSION LIMITING HINGES SHEARED AT THE HINGE PIN. THE ELEVATOR TRIM TABS WERE FOUND IN THE LANDING CONFIGURATION WITH TAB DEFLECTIONS AT ABOUT 9 DEGREES DOWN. THE RUDDER TRIM TAB WAS FOUND 20 DEGREES LEFT DEFLECTION. BOTH ENGINES WERE REMOVED TO AN ENGINE OVERHAUL FACILITY FOR DETAILED EXAMINATION. NO MECHANICAL DISCREPANCIES WERE FOUND AND POWER AND ROTATION SIGNATURES WERE EVIDENT. THE AIRPLANE WAS DEPARTING ON RUNWAY 11L FROM TAXIWAY 6 WITH A NINE KNOT TAILWIND AND 9950 FEET OF RUNWAY

Probable Cause: THE PILOTS IMPROPER PREFLIGHT INSPECTION, HIS FAILURE TO COMPELTELY SECURE THE AFT UTILITY DOOR, AND HIS FAILURE TO RECONFIGURE THE TRIM TABS TO A TAKEOFF SETTING. THE UTILITY DOOR'S SUDDEN OPENING JUST AFTER ROTATION AND THE EFFECT OF THE NOSE UP TRIM SETTING LED TO AN INADVERTENT STALL DURING THE TAKEOFF INITIAL CLIMB.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX93FA186
Status: Investigation completed
Duration: 6 months
Download report: Final report

Sources:

NTSB LAX93FA186

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
10-Apr-2024 14:28 ASN Update Bot Updated [Time, Operator, Other fatalities, Phase, Destination airport, Source, Narrative, Category, Accident report]

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