ASN Wikibase Occurrence # 35261
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 7 June 1994 |
Time: | 02:35 LT |
Type: | Mooney M20C |
Owner/operator: | Central Enterprises Inc. |
Registration: | N6879U |
MSN: | 2582 |
Year of manufacture: | 1963 |
Total airframe hrs: | 3472 hours |
Engine model: | Lycoming O-360-A1D |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | West Columbia, SC -
United States of America
|
Phase: | En route |
Nature: | Executive |
Departure airport: | |
Destination airport: | Swainsboro, GA (SBO |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE FLIGHT DEPARTED VIRGINIA LATE ON THE DAY BEFORE THE ACCIDENT AND ARRIVED IN SOUTH CAROLINA EARLY IN THE MORNING ON THE DAY OF THE ACCIDENT. AFTER REFUELING THE AIRPLANE WITH 10.1 GALLONS OF AVIATION FUEL, THE PILOT SPOKE BRIEFLY WITH THE FLIGHT LINE PERSONNEL. DURING THAT BRIEF CONVERSATION THE PILOT NEVER MENTIONED AN AIRCRAFT PROBLEM. WITHIN THIRTY MINUTES OF LANDING THE PILOT HAD REQUESTED AN INSTRUMENT FLIGHT CLEARANCE, AND DEPARTED. DURING THE INITIAL CLIMB RADIO CONTACT WAS LOST AFTER THE PILOT REPORTED THAT HE HAD A 'PROB'. ATTEMPTS BY THE AIR TRAFFIC CONTROLLER TO ESTABLISH RADIO CONTACT FAILED; RADAR CONTACT WAS NEVER ESTABLISHED. THE PILOT DID NOT EXPRESS WHAT TYPE PROBLEM HE WAS EXPERIENCING. EXAMINATION OF THE AIRCRAFT DID NOT REVEAL EVIDENCE OF A MECHANICAL MALFUNCTION. THERE WAS NO EVIDENCE OF PILOT IMPAIRMENT OR INCAPACITATION. ACCORDING TO THE LOCAL WEATHER OBSERVATION, INSTRUMENT WEATHER CONDITIONS PREVAILED AT THE TIME OF THE ATTEMPTED NIGHT FLIGHT.
Probable Cause: THE PILOT'S FAILURE TO MAINTAIN CONTROL OF THE AIRPLANE DURING CLIMBOUT BECAUSE OF SPATIAL DISORIENTATION. FACTORS WERE LOW CEILINGS AND THE DARK NIGHT.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL94FA116 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB ATL94FA116
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
10-Jan-2019 19:28 |
BEAVERSPOTTER |
Updated [Time, Cn] |
10-Apr-2024 07:02 |
ASN Update Bot |
Updated [Time, Cn, Operator, Other fatalities, Destination airport, Source, Narrative, Category, Accident report] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation