ASN Wikibase Occurrence # 35564
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Date: | Saturday 21 November 1992 |
Time: | 11:35 LT |
Type: | Beechcraft A60 Duke |
Owner/operator: | Huber, James D. |
Registration: | N100EK |
MSN: | P-209 |
Year of manufacture: | 1972 |
Engine model: | Lycoming TIO-541-E1C4 |
Fatalities: | Fatalities: 6 / Occupants: 6 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Snoqualmie Pass, WA -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Seattle, WA (KBFI) |
Destination airport: | Pullman, WA (KPUW) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:WHILE CLIMBING IN MOD ICING CONDS AFTER TAKEOFF, PLT WAS CLEARED TO 17,000'. RADAR DATA SHOWED ACFT CLIMBED AT AN INDCD AIRSPEED (IAS) OF 82 TO 123 KTS. A BEECH SAFETY INFO BOOKLET STATED THAT A MIN AIRSPEED OF 140 KTS MUST BE MAINTAINED IN ICING CONDS. CLIMBING AT REDUCED AIRSPEED WOULD HAVE INCREASED ANGLE OF ATTACK & ALLOWED ICE TO ACCUMULATE UNDER THE WINGS & AFT OF THE DE-ICING BOOTS. ACFT CLIMBED TO 13,500', DESCENDED MOMENTARILY TO 13,300', THEN CONTINUED CLIMBING AS AIRSPEED DECREASED ABRUPTLY. AFTER SLOWING TO 60 KTS IAS AT 13,700', THE ACFT ENTERED A STEEP DESCENDING TURN & ACCELERATED TO HIGH SPEED (ABOVE VNE). AN EMERGENCY WAS DECLARED, STATING THE AIRCRAFT 'LOST AN ENGINE.' SOON THERE- AFTER, RADAR CONTACT WAS LOST & THE ACFT CRASHED. PIECES OF EMPENNAGE SURFACES SEPARATED IN FLIGHT & WERE FOUND AT REMOTE LOCATION FROM THE MAIN WRECKAGE. BOTH COUNTERWEIGHTS SEPARATED FROM THE ELEVATORS. POST-CRASH TESTS DISCLOSED NO MECHANICAL EVIDENCE OF ENGINE MALFUNCTION. LOW CEILING, FOG, LIGHT RAIN, SNOW & ICING CONDITIONS WERE RPRTD IN AREA.
Probable Cause: FAILURE OF THE PILOT TO MAINTAIN CONTROL OF THE AIRCRAFT, HIS FAILURE TO PREVENT THE AIRCRAFT FROM EXCEEDING THE NEVER EXCEED SPEED (VNE), AND SUBSEQUENT EXCEEDING OF THE DESIGN STRESS LIMITS OF THE AIRCRAFT. FACTORS RELATED TO THE ACCIDENT WERE: WEATHER CONDITIONS (INCLUDING ICING CONDITIONS), IMPROPER AIRSPEED, AND LOSS OF ENGINE POWER FOR UNDETERMINED REASON(S).
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA93FA026 |
Status: | Investigation completed |
Duration: | 1 year and 7 months |
Download report: | Final report |
|
Sources:
NTSB SEA93FA026
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:22 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
10-Apr-2024 16:42 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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