ASN Wikibase Occurrence # 35865
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Date: | Wednesday 5 January 1994 |
Time: | 20:29 LT |
Type: | Beechcraft B90 King Air |
Owner/operator: | Kimura, Toyoshi |
Registration: | N230TW |
MSN: | LJ-445 |
Year of manufacture: | 1969 |
Total airframe hrs: | 7072 hours |
Engine model: | P&W PT6A-20 |
Fatalities: | Fatalities: 10 / Occupants: 10 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Okeechobee, FL -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Kissimmee, FL (KISM) |
Destination airport: | Opa-locka, FL (KOPF) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT (OR PILOT-RATED PASSENGER) REPORTED AN 'INDICATION' PROBLEM & SAID THEY INTENDED TO LAND AT OKEECHOBEE, BUT COULDN'T FIND THE AIRPORT. THEY THEN REPORTED ENGINE TROUBLE & SAID THAT THEY WOULD TRY TO LAND ON A ROAD. THEY CIRCLED THE AREA & APPROACHED A DIRT ROAD WITH LANDING LIGHTS ON. A CAR WAS PROCEEDING ON THE ROAD IN THE OPPOSITE DIRECTION. THE PLANE BEGAN TO CLIMB, & IT ENTERED A LEFT TURN. IT THEN ROLLED INTO A STEEP RIGHT BANK, DESCENDED NOSE DOWN, CRASHED & WAS CONSUMED BY FIRE. AN EXAM REVEALED INDICATIONS THAT BOTH ENGINES WERE OPERATING AT HIGH RPM. A TEARDOWN REVEALED A RIGHT ENGINE FUEL CONTROL BEARING HAD FAILED, WHICH WOULD HAVE ALLOWED IMPROPER MOVEMENT OF THE FUEL CONTROL DRIVE SHAFT. THE PLANE WAS LAST INSPECTED ON 11/25/92 & WAS 13 HRS OVER A REQUIRED 150 HR INSPECTION. A SERVICE BULLETIN FOR MAINTENANCE OF THE FUEL CONTROL BEARINGS HAD NOT BEEN COMPLIED WITH. THE OWNER/PILOT HAD NOT COMPLETED FORMAL GROUND SCHOOL INSTRUCTION ON THE AIRPLANE SYSTEMS & OPERATION. THE PLANE HAD 9 SEATS; 10 OCCUPANTS WERE ABOARD.
Probable Cause: THE PILOT'S IMPROPER REMEDIAL ACTION CONCERNING A RIGHT ENGINE POWER ANOMALY, AND HIS FAILURE TO MAINTAIN ADEQUATE AIRSPEED DURING GO-AROUND FROM AN ABORTED PRECAUTIONARY LANDING, WHICH RESULTED IN A LOSS OF AIRCRAFT CONTROL AND AN UNCONTROLLED DESCENT. FACTORS RELATED TO THE ACCIDENT WERE: FAILURE OF THE OWNER/OPERATOR/PILOT TO ASSURE PROPER MAINTENANCE INSPECTION OF THE AIRCRAFT, FAILURE TO COMPLY WITH A SERVICE BULLETIN CONCERNING THE ENGINE FUEL CONTROLS, SUBSEQUENT BEARING FAILURE IN THE RIGHT ENGINE FUEL CONTROL, AND THE PILOT'S LACK OF FAMILIARITY WITH THIS MAKE AND MODEL OF AIRCRAFT.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA94MA048 |
Status: | Investigation completed |
Duration: | 1 year and 5 months |
Download report: | Final report |
|
Sources:
NTSB MIA94MA048
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
22-Jan-2011 15:49 |
harro |
Updated [Aircraft type, Other fatalities] |
21-Dec-2016 19:22 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
14-Apr-2021 13:49 |
Captain Adam |
Updated [Operator, Departure airport, Destination airport, Narrative] |
10-Apr-2024 09:21 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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