Accident Monnett Sonerai N7037J,
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ASN Wikibase Occurrence # 36857
 
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Date:Friday 30 August 1996
Time:12:30 LT
Type:Silhouette image of generic SRAI model; specific model in this crash may look slightly different    
Monnett Sonerai
Owner/operator:Michael D. Michael
Registration: N7037J
MSN: 547
Total airframe hrs:90 hours
Engine model:Volkswagen 3-29
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Destroyed
Category:Accident
Location:Jeffersonville , IN -   United States of America
Phase: Unknown
Nature:Executive
Departure airport:Seymour, IN (KSER)
Destination airport:(KJVY)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot's airplane was #2 in a 4-airplane ferry formation of Formula V Class racing airplanes. The #3 pilot said that the #2 pilot's flying was erratic during the flight. 'He had a hard time staying in position. He would fly ahead, then drop back.' The witness said when they were within a mile of the landing airport, [the pilot] 'pulled straight up, pulled left to the east at full power, then went into a slight descent.' The witness said that he flew up along side of the pilot's airplane to try and get his attention. 'I couldn't get his eye. He would not even look at me. I chased him about 5 miles before I lost sight of him. The last time I saw him, he was below 500 feet.' Examination of the wreckage revealed that the adhesive resin which bound the rubber stripping forming the firewall lower seal was missing. The airplane had been involved in 2 earlier landing accidents, and had been repaired/inspected by pilots/mechanics of the racing association. The pilot/mechanic performed the annual inspection on 5/1/96. Two days before the accident flight the pilot said that he experienced smoke in the cockpit. He also said that the temperature was '185 degrees' and that he was very hot. The results of FAA toxicology specimens from the pilot revealed a carboxyhemoglobin saturation of 41.000 percent in the blood; loss of consciousness is attained at approximately 30.000 percent.

Probable Cause: inadequate maintenance and inspection of the airplane by the pilot/owner and other airframe and powerplant mechanics, which failed to assure adequate sealing of the engine firewall, and led to the pilot's incapacitation due to carbon monoxide.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CHI96FA322
Status: Investigation completed
Duration: 1 year and 6 months
Download report: Final report

Sources:

NTSB CHI96FA322

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:23 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
08-Apr-2024 19:19 ASN Update Bot Updated [Time, Operator, Other fatalities, Phase, Departure airport, Destination airport, Source, Narrative, Category, Accident report]

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