ASN Wikibase Occurrence # 36878
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Date: | Sunday 15 June 1997 |
Time: | 09:34 LT |
Type: | Cessna 172N |
Owner/operator: | Sky Portraits, Inc. |
Registration: | N738YG |
MSN: | 17270337 |
Year of manufacture: | 1978 |
Total airframe hrs: | 4973 hours |
Engine model: | Lycoming O-320-H2AD |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Greenbrier, AR -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Unknown |
Departure airport: | Fort Smith, AR (KFSM) |
Destination airport: | Jonesboro, AR (KJBR) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During an aerial photography flight maneuver, the airplane impacted power lines (35' high) and trees (40' high) during an uncontrolled descent. Witnesses heard the aircraft engine, did not recall any discrepancies with the aircraft, and observed the airplane maneuvering in the area of power lines, trees, and a water tower (92' high). The commercial pilot flew his initial 10 hours of aerial photography with a company photographer (formerly a company pilot). Company guidelines stated, in part, that the pilot is required to adjust altitude and radius according to the 'photographer's command.' The company operated without a flight department head and none of the company management personnel were pilots or mechanics. There were no written guidelines for training or pairing of pilots and photographers. There was no formal pilot flight training curriculum specific to the type of flying. Aircraft records did not reveal any anomalies or uncorrected maintenance defects. Examination of the airplane did not reveal any anomalies that would have contributed to the accident. Flight control continuity was confirmed to the flight control surfaces. The flaps were in the retracted position. Toxicology was negative.
Probable Cause: The pilot's failure to maintain aircraft control during a low altitude maneuver. Factors were the pilot's lack of total experience in the type of operation and inadequate training by the company management.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW97FA221 |
Status: | Investigation completed |
Duration: | 10 months |
Download report: | Final report |
|
Sources:
NTSB FTW97FA221
History of this aircraft
Other occurrences involving this aircraft Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
08-Apr-2024 14:52 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative, Accident report] |
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