ASN Wikibase Occurrence # 37184
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Date: | Friday 1 November 1996 |
Time: | 17:50 LT |
Type: | Mooney M20J |
Owner/operator: | Ellington Field Aero Club, Inc |
Registration: | N25LS |
MSN: | 24-0296 |
Total airframe hrs: | 2447 hours |
Engine model: | Lycoming 10-360-A1B6D |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | San Leon, TX -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | Houston, TX (KEFD) |
Destination airport: | Galveston, TX (KGLS) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A witness observed the airplane in a 3 to 4 turn (360 degree) spin to the right with the engine pointing downward before the airplane impacted the water and a fire erupted. The pilot received a 2.1 hour check out including stalls. He wanted to fly the airplane solo before beginning his commercial pilot training and rented the airplane for the local flight. Numerous entries for stalls were entered in the pilot's logbook; however, there were no entries for spin training (not required by FAR's). The pilot logged 6.4 hours of simulated instrument flight and 0.8 hour in actual instrument conditions during the 90 days prior to the accident. Radar summary charts indicated precipitation intensity levels throughout the area with tops to 30,600 feet. Weather stations reported wind gusts to 25 knots. Cumulus and towering cumulus clouds with multiple cloud layers associated with a front prevailed throughout the area. Convective sigmet and Airmets were in effect for thunderstorm activity, IFR ceilings and visibility. VFR flight was not recommended away from the local airport. There was no evidence of an inflight fire. Examination of the airplane did not reveal any pre-impact discrepancies.
Probable Cause: The pilot's inadvertent stall and spin of the airplane. Factors were the pilot's lack of total experience in the make and model of airplane and the weather conditions.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW97FA032 |
Status: | Investigation completed |
Duration: | 1 year and 5 months |
Download report: | Final report |
|
Sources:
NTSB FTW97FA032
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
08-Apr-2024 18:14 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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