ASN Wikibase Occurrence # 37884
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Date: | Saturday 26 October 1985 |
Time: | 10:13 |
Type: | Bede BD-5B |
Owner/operator: | private |
Registration: | N548BD |
MSN: | 548 |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Cape Girardeau , MO -
United States of America
|
Phase: | En route |
Nature: | Unknown |
Departure airport: | (CGI) |
Destination airport: | (CGI) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE OWNER/BUILDER HAD HIRED THE PLT TO TEST FLY THE ACFT ON ITS INITIAL flight. SHORTLY AFTER TAKEOFF, THE PLT TRANSMITTED THAT HE HAD AN ENG PROBLEM. HE WAS CLEARED FOR AN IMMEDIATE LANDING & ENTERED A DOWNWIND FOR RWY 28. AS HE CONTINUED & WAS TURNING FROM A BASE TO FINAL APCH, THE ACFT ENTERED A SPIN IN THE OPPOSITE DIRECTION. THE ACFT IMPACTED ON THE EDGE OF AN INTERSTATE HIGHWAY WHILE IN A STEEP NOSE-DOWN ATTITUDE. AN EXAM OF THE ENG REVEALED THE #1 CYCLINDER SPARK PLUG WIRE WAS COMPLETELY DETACHED; THE #2 CYLINDER WIRE WAS DETACHED FROM THE SPARK PLUG (ALTHO ITS DUST BOOT WAS STILL CONNECTED); & THE #4 SPARK PLUG WIRE DUST BOOT SHOWED EVIDENCE OF HAVING COME IN CONTACT WITH AN ADJACENT EXHAUST STACK & WAS BURNED UNTIL THERE WAS SEPARATION AT THE BOOT'S MIDPOINT. CAUSE:
Sources:
NTSB:
https://www.ntsb.gov/ntsb/brief.asp?ev_id=20001214X38102 Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
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