ASN Wikibase Occurrence # 38212
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Date: | Saturday 18 September 1999 |
Time: | 13:00 LT |
Type: | Piper PA-24-180 |
Owner/operator: | Joseph W. Burton |
Registration: | N5673P |
MSN: | 24-745 |
Engine model: | Lycoming O-360-A1A |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | June Lake, CA -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Petaluma, CA (069) |
Destination airport: | Bryce Canyon, UT (BCE |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot departed on a multi state cross-country flight and was reported missing when the airplane failed to arrive at the destination. The pilot originally had filed an IFR flight plan the night before his proposed departure and also obtained a weather briefing. The weather information contained in the briefing was substantially correct. He was delayed due to fog from his estimated time of departure and never refiled or opened the flight plan. CAP search aircraft located the wreckage 1 week after the accident. The aircraft was found at the 11,760-foot level of a mountain and about 1,000 feet below the peak. The site is about 2 miles south of the route of flight filed in his flight plan. Ground witnesses said there were gusty winds, heavy rain, and thunderstorms in the area the day of the crash, with clouds obscuring the mountaintop where the accident occurred. In his flight plan, the pilot had originally filed for 13,000 feet, and pilot reports during the morning and early afternoon indicated that the cloud bases were 10,000 to 12,000 feet over the mountains, with higher layers to 24,000 feet. Conditions were favorable for light to moderate clear and/or mixed icing in clouds and precipitation above 12,000 feet. No preimpact mechanical malfunctions or failures were found during examination of the airframe and engine. A review of the pilot's logbook indicated that he had 223 hours of actual instrument time and 71 hours of simulated instrument time. About 4 months preceding the accident, he had logged 3 hours.
Probable Cause: The pilot's continued VFR flight into known instrument meteorological conditions, including icing, which resulted in an in-flight collision with mountainous terrain.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX99FA316 |
Status: | Investigation completed |
Duration: | 1 year and 7 months |
Download report: | Final report |
|
Sources:
NTSB LAX99FA316
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
14-Dec-2017 09:26 |
ASN Update Bot |
Updated [Operator, Source, Narrative] |
07-Apr-2024 17:53 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Phase, Destination airport, Source, Narrative, Category, Accident report] |
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