Accident Rutan VariEze N13WM,
ASN logo
ASN Wikibase Occurrence # 38422
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Monday 18 October 1999
Time:10:10 LT
Type:Silhouette image of generic VEZE model; specific model in this crash may look slightly different    
Rutan VariEze
Owner/operator:John B. Cannon
Registration: N13WM
MSN: 218
Engine model:Lycoming O-320-B1A
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Quemado, NM -   United States of America
Phase: En route
Nature:Private
Departure airport:St. Johns, AZ (KSJN)
Destination airport:Albuquerque, NM
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
While visiting a repair facility in California to have minor repair work performed on the aircraft, the pilot was visited at his request by a man who sold him the engine's carburetor foam air filter. The man inspected the filter and it appeared 'aged' and 'crumbly.' The pilot declined to have the filter replaced, and the pilot then reinstalled it. After an overnight stop in Arizona while en route back to his home town in Texas, the pilot contacted Albuquerque ARTCC and reported a rough running engine. He requested vectors to the closest airport, but was never identified on radar. The last transmission from the pilot was received at 1008, and the aircraft was located by a local rancher several hours later. The airplane was landed on a dry dirt field parallel to a forrest road and directly perpendicular to another gravel road. The touchdown speed was estimated to be excess of 100 knots, and the aircraft's owners manual recommends 55 knots on a rough field. Following the accident, the engine was test run. Black smoke exited from the exhaust and the engine ran rough. An internal examination of the carburetor revealed that the foam air filter had been torn and pulled through the throat of the injector, causing a restriction in airflow.

Probable Cause: The pilot's selection of an unsuitable landing area on which to make a precautionary landing, and his excessive airspeed during landing touchdown. Factors were the ingestion of the foam air filter into the throat of the injector, and the pilot's failure to replace the worn air filter.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DEN00FA007
Status: Investigation completed
Duration: 1 year
Download report: Final report

Sources:

NTSB DEN00FA007

History of this aircraft

Other occurrences involving this aircraft
8 April 1995 N13WM Private 0 Addison, TX sub

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:23 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
14-Dec-2017 09:40 ASN Update Bot Updated [Operator, Departure airport, Source, Narrative]
27-Jul-2019 07:15 Anon. Updated [Narrative]
07-Apr-2024 17:18 ASN Update Bot Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org