Accident Taylorcraft BC-12D N43778,
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ASN Wikibase Occurrence # 39117
 
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Date:Saturday 12 December 1998
Time:17:30 LT
Type:Silhouette image of generic TAYB model; specific model in this crash may look slightly different    
Taylorcraft BC-12D
Owner/operator:Private
Registration: N43778
MSN: 7437
Total airframe hrs:3317 hours
Engine model:Continental A-65-8
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Greenville, PA -   United States of America
Phase: Take off
Nature:Training
Departure airport:, PA (4G1)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
A witness reported that the student pilot had been in the traffic pattern for 15 - 20 minutes during his second flight of the day. A second witness, who was in the pattern at the time of the accident, reported seeing the aircraft touch down in a grassy landing area to the right of, and parallel to, paved runway 15. It then veered left, crossed runway 15, and continued towards a large briar patch and an intersecting turf runway, during which the aircraft entered a steep, climbing left turn. The witness reported that he then observed the aircraft nose drop, and 'go over.' A third (ground) witness reported seeing the aircraft cross over the briar patch and make a climbing left turn which was described as 'not excessively steep', and with the angle of bank of at least 25 degrees. This was followed by the aircraft leveling off, and then impacting trees. This witness reported the winds as calm. On site examination revealed that the aircraft first encountered trees approximately 10 feet below the 70 foot high tops, and the wreckage distribution progressed toward 030 degrees magnetic to ground impact. There was no evidence of pre-impact control or engine malfunction. The student pilot had 109 total flight hours. He had some initial flight training in 1944, then began flying again in 1995.

Probable Cause: The pilot's failure to maintain directional control during touch-and-go landing, and his failure to maintain obstacle clearance. A factor was the tree.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: NYC99FA037
Status: Investigation completed
Duration: 1 year 1 month
Download report: Final report

Sources:

NTSB NYC99FA037

History of this aircraft

Other occurrences involving this aircraft
28 April 1990 N43778 Private 0 Meadville, PA sub

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:23 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
04-Apr-2024 12:25 ASN Update Bot Updated [Time, Operator, Other fatalities, Departure airport, Source, Narrative, Category, Accident report]

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