ASN Wikibase Occurrence # 40748
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Date: | Sunday 30 September 1990 |
Time: | 14:20 |
Type: | Pierson Pusher |
Owner/operator: | private |
Registration: | N75FM |
MSN: | 1 |
Total airframe hrs: | 28 hours |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Kankakee, IL -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A HOMEBUILT AIRPLANE ON TAKEOFF CLIMBOUT WAS OBSERVED WITH MAIN GEAR RETRACTED AND NOSE GEAR EXTENDED. WITNESSES RECOUNT THE ENGINE SPUTTERING, FOLLOWED BY A STALL AND A UNCONTROLLED DESCENT TO GROUND. THE CARBURETOR CHOKE PLATE WAS FOUND CLOSED. THE PILOT HAD INSTALLED A POSITIVE DOWNLOCK ON THE NOSEGEAR TO PREVENT RETRACTION UNLESS A PULL-TO-RELEASE HANDLE IN THE COCKPIT WERE USED. THE HANDLE TO ENABLE NOSEGEAR RETRACTION RESEMBLED THE CHOKE HANDLE. CAUSE: A LOSS OF ENGINE POWER DUE TO ACTIVATION OF CARBURETOR CHOKE AND AN INADVERTENT STALL DURING THE FORCED LANDING.
Sources:
NTSB:
http://www.ntsb.gov/ntsb/brief.asp?ev_id=20001212X24208 Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
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