ASN Wikibase Occurrence # 40999
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Date: | Sunday 26 May 1985 |
Time: | 18:15 |
Type: | Globe GC-1B |
Owner/operator: | Ricky Randle Waliman |
Registration: | N80970 |
MSN: | 1163 |
Total airframe hrs: | 1819 hours |
Fatalities: | Fatalities: 1 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Moorpark, CA -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Oxnard, CA (CMA) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:ACFT CRASHED WHILE BEING MANEUVERED IN A CANYON. POST CRASH INSPECTION OF THE PROPELLER REVEALED NO EVIDENCE OF ROTATION AT IMPACT. ONE-HALF GAL OF AUTOMOTIVE FUEL WAS FOUND IN THE LEFT WING TANK AND NO FUEL WAS FOUND IN THE RIGHT WING TANK. SOME FUEL LINES WERE BROKEN AT THE CENTER WING AREA WHICH WOULD HAVE ALLOWED SOME LEAKAGE AFTER THE ACCIDENT, HOWEVER, THERE WAS NO EVIDENCE OF EXTREME AMOUNTS OF FUEL SPILLAGE IN AND AROUND THE ACFT. THE ENGINE WAS RUN TO FULL POWER AFTER THE ACCIDENT WITH NO EVIDENCE OF MECHANICAL FAILURE. THE ACFT'S FUEL VALVE WAS FOUND BETWEEN THE OFF AND ON POSITIONS, WHICH DID NOT ALLOW FUEL TO FLOW THROUGH IT, HOWEVER, THERE WAS EVIDENCE OF IMPACT DAMAGE TO THE VALVE. THE ACFT'S FUEL GAGE STILL READ ONE QUARTER FULL AFTER THE CRASH WITH NO FUEL IN THE ACFT. CAUSE:
Sources:
NTSB:
http://www.ntsb.gov/ntsb/brief.asp?ev_id=20001214X36492 Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:23 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
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