ASN Wikibase Occurrence # 41653
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Date: | Monday 23 September 1996 |
Time: | 17:00 LT |
Type: | Cessna U206G Stationair 6 |
Owner/operator: | Stearns Air Alaska |
Registration: | N7312C |
MSN: | U20603872 |
Total airframe hrs: | 2066 hours |
Engine model: | Continental IO-520-F |
Fatalities: | Fatalities: 3 / Occupants: 5 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Lake Hood Seaplane Base, Anchorage, AK -
United States of America
|
Phase: | Initial climb |
Nature: | Unknown |
Departure airport: | , AK (KLHD) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The aircraft (acft) took off from Lake Hood Seaplane Base with 5 occupants aboard. Witnesses said that after lift-off, flaps were retracted & acft pitched to a climb attitude; but stopped climbing & began settling, then struck a utility pole at the airport boundary. It then crashed on a road, & a fire erupted. Calculations showed acft was within allowable weight & balance parameters. Engine exam revealed brass throttle arm (PN 632555-23) was worn & had disconnected from the throttle linkage. It had disconnected where a hard steel bushing (with splines) had been installed (pressed) in a mounting hole in the relatively soft throttle arm. The mounting hole had become 'U' shaped with one side open. The opening was large enough to allow passage of the throttle linkage connecting bolt & bushing. Deposits of material from the throttle arm were found on the bushing splines. The deposits were consistent with rotational motion of the bushing within the mounting hole, as if rotation occurred while tightening the bolt. Teledyne Continental Service Bulletin SB95-2, dated 4/21/95, provided inspection & lubrication procedures for throttle linkages at each 100 hr, progressive, and/or annual inspection. Acft had been flown 80 hrs since its previous (annual) inspection on 8/11/96.
Probable Cause: improper installation of a connecting bolt in the throttle linkage, which resulted in a worn/disconnected throttle arm, partial loss of engine power, and a forced landing after takeoff.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ANC96FA162 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB ANC96FA162
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
29-Nov-2015 10:28 |
JINX |
Updated [Location, Phase, Nature, Departure airport, Destination airport, Source] |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
13-Oct-2017 18:45 |
TB |
Updated [Aircraft type, Cn, Location] |
08-Apr-2024 18:52 |
ASN Update Bot |
Updated [Time, Cn, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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