ASN Wikibase Occurrence # 41846
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Date: | Sunday 28 December 1997 |
Time: | 20:30 LT |
Type: | Cessna 177 Cardinal |
Owner/operator: | Charles D. Coffman |
Registration: | N30255 |
MSN: | 17701153 |
Engine model: | Lycoming O-320-E2D |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Fort Leonardwood, MO -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Audubon, IA (KAUD) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The non-instrument rated pilot obtained outlook and abbreviated weather briefings before departing on an extended cross country. During the abbreviated weather briefing the FAA's FSS specialist advised the pilot that '...VFR flight is not recommended.' The pilot said he would call the FAA FSS back before departure. There was no record of a return call by the pilot. Later in the day, the pilot landed at an airport midway between his departure airport and planned destination. While at the airport he refueled the airplane and obtained a weather briefing. The pilot told the airport manager that the FSS specialist told him that VFR flight was not recommended. The manager suggested the pilot fly south into eastern Kansas, west of the weather system, land and check the weather before continuing. Relatives reported the pilot missing on December 28, 1997. The airplane was found on April 17, 1998. The on-scene examination revealed the airplane collided with trees, terrain and was destroyed by fire. Examination of the airframe, engine and flight control system revealed no anomalies that would have prevented flight. Weather reported about 60 miles southwest and 35 miles northeast of the accident site showed IMC conditions at the approximate time of the accident.
Probable Cause: The pilot's failure to maintain adequate obstacle clearance and his inadequate inflight decision which resulted in VFR flight in to instrument meteorological conditions. The pilot's overconfidence in his ability is a contributing factor.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI98LA126 |
Status: | Investigation completed |
Duration: | 2 years and 2 months |
Download report: | Final report |
|
Sources:
NTSB CHI98LA126
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
04-Jun-2023 01:18 |
Ron Averes |
Updated [[Time, Damage, Category, Investigating agency]] |
08-Apr-2024 11:15 |
ASN Update Bot |
Updated [Time, Cn, Operator, Other fatalities, Departure airport, Source, Narrative, Category, Accident report] |
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