Accident Cessna 150D N6052T,
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ASN Wikibase Occurrence # 42338
 
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Date:Saturday 16 July 1994
Time:09:40 LT
Type:Silhouette image of generic C150 model; specific model in this crash may look slightly different    
Cessna 150D
Owner/operator:Douglas Kiss
Registration: N6052T
MSN: 15060752
Total airframe hrs:2980 hours
Engine model:Lycoming O-320-E2D
Fatalities:Fatalities: 2 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Carrville, CA -   United States of America
Phase: En route
Nature:Private
Departure airport:Lincoln, CA (O51)
Destination airport:Portland, OR
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
THE FLIGHT WAS EN ROUTE TO PORTLAND OVER MOUNTAINOUS TERRAIN. AT 0940, THE U.S. FOREST SERVICE WAS NOTIFIED OF A FIRE AND THE AIRCRAFT WRECKAGE WAS SUBSEQUENTLY LOCATED IN A SADDLE AT THE 6,480-FOOT LEVEL. THE ACCIDENT SITE IS THE ONLY RELATIVELY CLEAR AREA IN THE VICINITY. AT 1000, A HELICOPTER REACHED THE ACCIDENT SITE AND DROPPED WATER ON THE BURNING WRECKAGE. THE WRECKAGE WAS FOUND WITHIN A 23-FOOT-DIAMETER AREA. AN EXAMINATION OF THE AIRCRAFT WRECKAGE REVEALED DAMAGE CONSISTENT WITH A LOW-SPEED, MODERATE-ANGLE CONTROLLED IMPACT. THE AIRCRAFT'S ENGINE HAD BEEN MODIFIED TO OPERATE ON 87 OCTANE AUTO FUEL. AN INSPECTION REVEALED THE SPARK PLUGS WERE WORN, WITH THE ELECTRODES FOUND TO HAVE A GAP IN EXCESS OF .022 OF AN INCH. NONE OF THE SPARK PLUGS WERE FOULED. THE FUEL INLET SCREEN EXHIBITED A DARK, WET SUBSTANCE. A THREAD COMPOUND WAS PRESENT AND ON THE FUEL INLET SCREEN. THE CARBURETOR HAD COMPOSITE FLOATS INSTALLED. THE TWO-PIECE VENTURI WAS FOUND DISPLACED IN THE CARBURETOR THROAT. A LINEMAN AT LINCOLN HAD SEEN THE AIRCRAFT BEING FUELED FROM SEVERAL CANS THE DAY PRIOR TO ITS DEPARTURE FROM THE LINCOLN AIRPORT.

Probable Cause: a loss of engine power for undetermined reasons. The mountainous terrain and lack of a suitable forced landing area within gliding distance was a factor in the accident.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX94LA286
Status: Investigation completed
Duration: 8 months
Download report: Final report

Sources:

NTSB LAX94LA286

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:24 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
10-Apr-2024 05:58 ASN Update Bot Updated [Time, Other fatalities, Source, Narrative, Category, Accident report]

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