ASN Wikibase Occurrence # 42827
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Date: | Wednesday 17 December 1997 |
Time: | 15:54 LT |
Type: | Beechcraft C35 Bonanza |
Owner/operator: | Charles A. Keown |
Registration: | N782D |
MSN: | D-3051 |
Total airframe hrs: | 5287 hours |
Engine model: | Continental E-225-8 |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Evansville, IN -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | (3EV) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane hit the tops of trees located about 280 feet from the impact site on the side of a highway berm. The descent angle measured eight degrees. The left wing hit two small trees located 17 feet in front of the initial ground scar. The airplane spun around and came to rest 9 feet from end of the initial ground scar. No propeller ground scars were found. One propeller blade was undamaged. The other blade was undamaged except it had 4 inches of chordwise scratching on the backside of the blade. The examination of the airplane revealed flight control and engine continuity. The fuel system on the engine had been converted to a fuel injection system. The fuel in the airplane was autogas. A green hose was found connecting the fuel line at the fire wall to the engine driven fuel pump. The fuel line was marked, 'GATES 6C5D FLEXLINE 5/16 INCH 1500 PSI MAX HYD WP MADE IN USA.' The manufacturer of the green hose reported it was a common hose used for petroleum products such as transmission fluid or anti-freeze. The manufacturer reported it had not made aviation hoses for many years. Inspection of the green hose revealed that the B nut attached to the fire wall was loose. A witness reported that the pilot performed maintenance on the airplane, although he was not an Airframe and Powerplant mechanic.
Probable Cause: Improper maintenance by the use of a loose fitting unapproved fuel line, which resulted in fuel starvation and the loss of engine power.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI98FA068 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB CHI98FA068
Location
Revision history:
Date/time | Contributor | Updates |
24-Oct-2008 10:30 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
08-Apr-2024 11:28 |
ASN Update Bot |
Updated [Time, Operator, Other fatalities, Phase, Source, Narrative, Category, Accident report] |
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